OSRAM AD838L / AD830R
Globetronics AD8930UV
outstanding issue update
09072009
Tony Lui
Objective
Buyoff :
Clear OSRAM AD838L CTM OSL before 9/9
Clear OSRAM AD830R OSL
General support:
Solve Globetronics AD8930UV(April 06) hard disk corrupt cannot startup
issue
Solve Inari AD830, AD838 OSL
Multi-chip verify in Inari AD830
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 2
OSRAM AD838L CTM Outstanding List update
SW (CTM stated payment deadline 9/9) ---------SW 7.00.29 will release on 9/9 4:00p.m.
Epoxy search boundary display
Available, however displayed boundaries stay on screen and display position shifted
Panel exist sensor SW
If 1st slot panel exist error during loading magazine upper platform pusher not return, align pusher not on
Clear track more than once sometimes hold up at testbond screen (9/3)
1 die wafer search
st
Global align angle message not close after Change wafer
Stamping module crash issue
After upgraded to 7.00.27 and go to stamping position page, temp. solved if LF data page refreshed
Dispense LF map enable scenario is reported by A.H.Tan, solved in 7.00.25
Access level amendment request by CTM in ww35: technician mode need to able to access exit
(New) Magazine tilt sensor, if tilted, track not clear next time, 2 LF jammed afterwards.
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 3
OSRAM AD838L CTM Outstanding List update
HW
Polarizer light box
Setting test: Loose threshold settings under new panels mass run on Helios sampling
Dust, scratch and epoxy can be detected
0 wrong reject other than the above items in single panel 784 units
YT Lee Released new OPR of 01-67133-02, 01-67132 for the rest 4 field machines
Chan Koon Man released new DI for 2 new machines with the polarizer
New Vacuum cleaner (S/O:90543A01):
Hidy sent out on 9/8/2009, pending tracking number from Hidy
4th generation elevator guide(S/O: 90091):
9/9, Vincent Chan in-house modifying, 9/10/2009 will sent out
ESD material elevator rails (S/O:89338):
Originally 9/4/2009..pending
750um stamping pin (S/O:85263C01 for 2 new MC, S/O:90340 for field MC cancelled, S/O:90999):
9/11/2009..manufacturing issue..pending delivery
Operation, PM manual received on 9/9/2009 Open items
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 4
AD838L Polarizer Rejected case log verification on pre-bond
substrate inspection settings
Scratch
Foreign
material
Comment:
using 90% polarized blue ring light, 8 exposure, very loose setting,
Results positive, No over wrong reject inside the 10 reject unit1 panel test (784 units)
The rejected units were main scratch, Foreign material
Follow up: called 4 sets (01-67133-02 and 01-67132 ) in OPR and 2 sets in DI
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 5
AD838L Uplook verification
Condition:
7.00.15 SW, (7.00.27 unable to unlock uplook menu)
5x5 FOV uplook optics (conventional uplook optics is 3x3 FOV)
6x6 FOV bond optics
Local alignment
Calibration done on uplook:
COR
Zoom auto Calibration
Aligned uplook theta with Bond Arm X, Y axis (best align with substrate, however only BA is available for align)
According to Hei Man Previous report, Extra tighten the mounting screws and adjustment screws to verify
Post bond Results
Post bond results X SD, range Y SD, range T SD, range Uph
(um) (um) (degree)
Without Uplook 1.710, 8.960 2.360, 12.140 0.073, 0.36 6.7K
With Uplook 2.185, 9.650 2.279, 10.810 0.090, 0.44 5.8K
Comment: no significant changes in SD, ranges, UPH decreased 0.9K
Moreover, Y mean is shifted from -2 to -33 um after enabled uplook
Requested OSRAM side to measure in smartscope, pending results
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 6
Measurement result by smartscope
Smartscope measured with better results for uplook camera
Smartscope results X SD, range Y SD, range T SD, range Uph
(um) (um) (degree)
Without Uplook 6.7K
With Uplook 5.8K
uplook self test
’ø”©ú®
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 7
Results with/without uplook
Without uplook
With uplook
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 8
Panel crack reported by production 9/7/2009
2 panels cracked on Blizzard LED machine in 9/4
and 9/7 respectively
According to report by production
Kicker jam happen
2 Panel is jammed together during output
Observation
2 Panels crack at left border, 1 at top right corner and middle
Jam sensor working, if jam happens, system unable to continue
test run unless home kicker
Magazine tilt error will left substrate in track and no kick out
after tilt error
Suspected reason
SW
Action
Suggested record down operators action on the first jammed
substrate next time
Request SW debug for
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 9
AD830R OSL issues
Epoxy on die issue
On site SW verify on 9/7/2009, intermittently disconnect / block air tube 5 times with missing die/ BH clog
error generated normally, results positive for SW signal checking
Flow Signal tracking, suspected signal instability, results shows large bond delay has
S/O: 90419 flow sensor UGK sent from AAA on 9/7/2009
Plan install on 9/10
Meeting on 9/9/2009
Post bond 2 new stop mode SW test
Received SW on 9/8 night, plan to test 9/10
MC #51 SO board burnt for “no blow” solenoid, need replacement,
Plan to install on 9/10
UPH <12K in single row package issue
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 10
AD830R epoxy on die issue
Symptom
Epoxy on die happened in every 50K
3 mode of epoxy on die
Epoxy climb up at side of the die
Contaminated collet
Stacked die at bond side
Suspected reason
Epoxy too thick at epoxy disc side
Collet shift, collet decay
Machine unable to detect or alarm user after missing die/ BH clog
SW detection timing
Sensor Hardware sensitivity
Pneumatic stability
Mis-operation after missing die/ bond head clog
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 11
Observations
Collet is delicate
Collet is deformed from 5mil to 4mil ID (flow from 112 to 91) during
production
Die not at collet center
Found at 9/7/2009 morning, collet picked a die but missing die error
happened due to die shift and air leak
Wafer optics was found zoom in /out will shift ¼ of screen which is >30mil
Ejector hole is shifted, rotation of die also solved after adjustment
Ejector up level is too high
85um thick die is using 200um ejector up level
160 up level can pick up without missing die
Suggest to use 160 ejector up level
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 12
AD830R epoxy on die issue flow signal study
Flow control signal monitoring on 9/7/2009 on MC #51
About 65 ms after vacuum on again entering stable state
Refill
vacuum
Solenoid signal
Release overshoot
overshoot state
state
Stable
state
Flow sensor
Ideal Flow signal signal
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 13
Effect of vacuum flow by BHX, BHY, BHZ motion
Turn on vacuum and dry run BHX, BHY, BHZ
No observable difference on vacuum flow when BA is moving x,
y, z no blocking inside BA pneumatics
Testbond with
Idle state enable vacuum enabled
vacuum
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 14
Test condition
BHX, BHY, BHZ, BH valve turn on only without actual picking die
Wave Form
Bond delay< 22ms release vacuum overshoot is joining the refill vacuum overshoot
Bond delay >22ms
Bond
delay Bond
22ms delay
30ms
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 15
Suggested actions
Suggest use
Regarding to Trace the vision failure cases with the error log
together to know error generated or not during bad units
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 16
Globetronics AD8930UV Hard disk corrupt issue
Clone hard disk finished on 9/5/2009
Machine is able to initialize and modules configuration is customized for the old AD8930UV
Machine passed to technician for setup bonding
Output LF deform issue reported by technician
Before hard disk corrupt, the machine was found deform LF said by technician
Reasons: 1st slot position, column pitch, elevator column pitch not fine tune and rotation of
output elevator cassette, elevator missing steps
Action:
Finished fine tune position, pitches
Results:
can output for every slot without deform, occasionally Y missing step happens and need reset to restore
Suggested action
For missing steps of MMU elevator motors, suggest do PM on the machines, temporarily
can reset elevator once to restore missing steps
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 17
Inari AD830/AD838 CTM Outstanding List
update
HW
AD830 Piston for better epoxy level detection (Penang SO#: 250002017, S/O: pending):
Received, need demonstration to CTM on epoxy level detection
AD838 Window clamp for avoiding 1 st row hit collet (S/O:89925A02):
9/9 delayed, pending new delivery date
AD838 Fix clamp for avoid Substrate bring back(S/O:89925A02):
9/9 delayed, pending new delivery date
AD838 vacuum hole anvil block(S/O:89925A02):
9/9 delayed, pending new delivery date
AD838 wafer cover (S/O: 88539)
Cancelled
SW
AD830 Multi-chip feature debug… need verification with Process Cheah by A.H.Tan
AD830 SW standardization, (all AD830 should be capable to use latest SW, will do after multi-chip debug finish)
AD838 LF mark implementation… pending Tse Kai Yin, Tang Liang Hong
Internal discussions
Epoxy too large issue
Reset elevator magazine jam intermittently issue
SW: AD838 Clear bond track without clear memory intermittently.., cannot repeat in field and in-house, suggested Ronald demonstrate the issue to Tang
Liang Hong on 9/9
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 18
Inari AD830 epoxy dispense too large issue
Symptom
Dispensing epoxy coverage too large for their package
Even take epoxy filled nozzle to stamp without pressure, epoxy is already too large
Target coverage and dot size
4 side coverage without hitting border
In practical, around half die size epoxy will give a pass coverage, i.e. 300um dot size for
600um dies
Observation
Dispense epoxy shows normal coverage but already exceed pad border
For Sumitomo CRM 1295, the viscosity is lower than other package ablebond 8-41 epoxy,
300um epoxy ID nozzle will generate 400 um epoxy, which is too large for their 600um die
Inari Process Cheah feedback there was void inside syringe during material coming
Suspected reason
10 mil nozzle is too large to handle the CRM 1295 epoxy and to fulfill the small coverage
requirement in this package
Suggestion
CTM has 8mil, 10mil nozzles, suggest use a 8mil nozzle instead of 10mil to test
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 19
Parameters for 0 pressure “stamp” after nozzle
filled with epoxy
Pressure 0.003MPa, vacuum -1.0kPa
Pre-sqeeze delay: 50ms
Squeeze time: 3ms
Exhaust time: 3ms
Post squeeze delay: 3ms
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 20
Picture demonstration on Dot size large issue
Epoxy Filled Nozzle with 0 pressure “stamp”
Epoxy dot shape
Only the nozzle ID area has epoxy and already too large
Coverage
Normal coverage, just able to cover die corners
Epoxy too much and exceed the pad border
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 21
Schedule
AD838L OSL follow up
Continue checking panel crack issue
Global epoxy setup
Uplook smartscope measuring results
Installation and testing of 4th generation elevator guide (Sent out on 9/9)
Installation of vacuum cleaner x 5 on all field AD838L (Sent out on 9/8)
AD830R
Repair SO board
Test AD830R new post bond mode SW
Epoxy on die issue
Upgrade HW flow sensor on 9/10
Jan 10, 2023 ASM Pacific Technology Ltd. © 2009 page 22