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Big HEAD Pillow

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Telecommunications Case Studies Address Head-In-Pillow (Hnp)

Defects and Mitigation through Assembly Process Modifications and


Control

Russell Nowland
Alcatel-Lucent
14000 Quail Springs Parkway, Suite 300
Oklahoma City, OK 73134-2620, USA
E-mail: [email protected]
Phone: 405-302-1660

Richard Coyle and Peter Read


Alcatel-Lucent
600-700 Mountain Ave. Room 1E-247
Murray Hill, NJ 07974-0636, USA
Email: [email protected]
Phone: 908-582-8062

George Wenger
Andrew Division of CommScope
Senior Principal FMA/Reliability Engineer
Email: [email protected]
Phone: 908-546-4531

ABSTRACT
One of the most perplexing phenomena in the electronic manufacturing industry today is the defect called “head-in-pillow.”
Head-in-Pillow (HnP) defects occur on the blind solder joints of area array packages such as FBGAs, μBGAs and CSPs.
Often these insufficient or intermittent solder joint defects go undetected during manufacturing despite inspection with
conventional X-ray systems. They also are insidious reliability defects that often escape the normal testing procedures and
fail at the end user site. The head-in-pillow defects typically occur at the corner pins and outer rows of packages and are
associated with package warpage. There are new 3D imaging systems that can help detect this, but they rely on the operator
to interpret the images. There are BGA video inspection systems that can view under most devices, depending on the
standoff, but they are dependent on the access, viewing angle, and operator interpretation. These x-ray and video processes
also are very slow and costly.

There are several factors that can contribute to the head-in-pillow phenomena including package co-planarity, package
warpage, and assembly issues associated with solder paste characteristics and stencil printing. From a process standpoint, the
cause of the head-in-pillow often is the result of the sum of all of the component and assembly process tolerances. This paper
will discuss several contributing factors to the head-in-pillow defects and techniques to control them. It will include
reviewing DOE for solder paste deposition of five different pastes, Shadow Moiré scans on several problematic devices,
cross-section analysis of failed solder joints, and solder paste analysis of “head-in-pillow” pastes. The case studies presented
show that process control can mitigate HnP defects but may not be successful for some severe examples of HnP defects.

This paper uses components from telecommunication product case studies to demonstrate the effects of different contributing
factors and mitigation techniques for HnP defects. The case studies include reviewing solder paste printing modifications,
solder paste DOE, Shadow Moiré scans on several problematic BGA packages, effectiveness of x-ray inspection, and cross-
section analysis of failed HnP solder joints. Together, these case studies show that BGA package warpage is a major
contributor, but HnP defects can occur when almost any of the assembly process parameters deviate from acceptable
practices.
INTRODUCTION
There are several trends in the electronics industry that have increased the challenges of surface mount (SMT) board
assembly. These include conversion to Pb-free manufacturing, increased density at both the printed circuit board (PCB) and
package level, new package constructions, new laminate material sets, and thicker PCB constructions. One of the
consequences of the evolving and challenging technologies has been the increased occurrence of an open joint ball grid array
(BGA) defect called head-in-pillow [1-6]. This defect is known by many other names such as head-on-pillow, head-and
pillow, ball in cup, ball in socket, and hidden pillow. For the purpose of this paper, the defect will be referred to by the
acronym HnP.

The HnP phenomena are characterized by complete melting of both the solder paste and the BGA solder ball but with
insufficient coalescence to produce well-formed solder joints. Figure 1 shows examples of HnP defects using: a) an optical
photomicrograph of a typical HnP metallographic cross section and b) an optical photomacrograph of the outer row of a BGA
with an HnP defect. Figure 1a shows that the BGA ball sits on the solidified paste without forming a contiguous, well-formed
solder joint. These are latent defects that are not detected using standard manufacturing test methods such as visual inspection,
x-ray, and particularly electrical screening. The latter is important because these defects can pass in-circuit and functional test,
only to fail completely or give an intermittent connection after some period of deployment in service.

The increased frequency of HnP defects has coincided with a decrease in component interconnection pitch below 1mm, a
decrease in solder paste deposits below 6-mil thickness and an increase in processing temperature to accommodate Pb-Free
assembly. HnP is now recognized to the point that inspection systems and solder pastes are being developed to target this
problem. Additionally, standards development organizations are attempting to address this from a device standpoint [ref].
Despite these efforts, HnP defects have not been eliminated and in fact, probably are increasing because assembly process
windows are decreasing.

Typically, HnP defects are associated with the higher reflow temperatures used in Pb-free manufacturing. Although surface
contamination can cause HnP, it is more common for the defect to be attributed to the excessive component and PCB
warpage that results from higher temperature processing. This paper will use a number of case studies to illustrate that
sufficient warpage can occur in the SnPb reflow range as well as the Pb-free range resulting in HnP defects. The paper also
will discuss several contributing factors to the HnP defects and techniques used to mitigate or control them. This will include
reviewing DOE data for solder paste deposition of five different pastes, Shadow Moiré data on several problem devices,
cross-section analysis of failed solder joints, and a comparison of solder pastes used to mitigate HnP. The case studies
presented show that process control can mitigate HnP defects but may not be completely effective in some severe examples
of HnP defects.

Figure 1. Examples of HnP defects a) optical micrograph of solder joint cross section, and b) Side view of a row of BGA
balls with HnP at arrow.

HEAD-in-PILLOW DESCRIPTION
The HnP defects are created during the reflow process and have been described in the work by Amir et al (Intel [1]). Figure 2
shows pictorially how a gap develops between the ball and the solder paste due to dynamic warpage of the package or PCB.
If there is insufficient flux activity to remove the oxide coating on the surface of the ball, or there is some contamination on
the solder ball or molten solder paste mass, these two will not coalesce as shown in Figure 2d. The end result is an HnP
solder joint defect when the package cools below solidification (Figure 2e).
Figure 2. A pictorial representation of HnP defect formation (from Amir et al, reference 1).

CASE STUDY 1 – 144 I/O FINE PITCH BGA


Problem Description
In this application, the FBGA component exhibited extremely low yields (as low as 10%) when used in a complex
telecommunication printed circuit board assembly (PCBA). There were multiple SnPb 144 I/O FBGA components soldered
onto this PCBA and each had a unique pattern of HnP defects. Data provided by the device supplier indicated that this
component was not sensitive to HnP defects when used in high temperature, Pb-free solder assembly process. The basic
package pin diagram for the component is shown in Figure 3. Figures 4 and 5 show the defect maps and metallographic cross
sections for two devices that exhibited severe HnP open joint failures.

Figure 3. The package pin diagram for the 144 I/O FBGA.
Figures 4 and 5. Defect maps and metallographic cross sections for two SnPb FBGA (labeled BGA #1 and #2) devices that
exhibited severe HnP open joint failures.
A comparison of the defect maps for BGA #1 and #2 shows that an identical device can have very differently HnP signatures
when assembled onto two different locations of the PCBA. When warpage is the root cause of HnP, the defects
characteristically manifest themselves at the corner or outer row sites in BGA packages. While that is generally the case for
these two BGAs, their defects are not limited to the corners or edges of the packages. It also is very obvious that the number
of defects varies and the defect patterns are not symmetric for the two packages.

Figure 6 shows one of the HnP defects from BGA #1 at higher magnification. These photomicrographs illustrate the potential
latent character of the HnP defects. There is good mechanical contact at the interface between the solidified ball and the paste
even though there is no coalescence across the interface. This site is located on an inner row and is not likely to be detected
with a visual or a detailed microscopic inspection. It definitely will pass electrical testing and may pass thermal screening if
adjacent sites are properly soldered and support the integrity of the mechanical connection.

Figures 6. These photomicrographs illustrate the latent nature of the SnPb HnP defects. There is good mechanical contact at
the interface between the solidified ball and the paste even though there is no coalescence across the interface.

Root Cause Analysis


The defects are located not only at or near the outside of the package, but also outside the die shadow (see Figures 4 and 5).
Contamination would be expected to produce a less localized pattern of detects, which focuses attention on package warpage
as the most probable root cause of the HnP defects. Table 1 shows a summary of Shadow Moiré warpage [7] measurements
on the 144 I/O FBGA package. There are a number of notable observations in these data. First, the peak warpage occurs at
the SnPb (not Pb-free) peak soldering temperature. Second, the warpage is not symmetric around the peak temperature. Third,
the warpage is not completely reversible or recoverable following the simulated reflow temperature cycling. Finally, although
the room temperature warpage or coplanarity is 70-80 μm (3-4 mils) is quite acceptable, the warpage is substantially greater
at the high temperatures in the reflow profile warpage, where HnP is known to occur.

These data do not describe or account for any asymmetry in warpage across the package. Measurements on other similar
FBGA packages show similar but not absolutely identical results, thus some of the variation in the defect patterns between
BGA #1 and BGA #2 could be the result of package-to-package variations. However, the type of statistical studies need to
verify those variations is beyond the scope of this work. It should also be noted that these package warpage measurements
obviously can not account for additional effects due to PCB warpage.
Table 1. A summary of Shadow Moiré warpage measurements on the 144 I/O FBGA package. Note that the peak warpage
occurs at SnPb, not Pb-free soldering temperatures.
Temperature Warpage
°C μm
30 70
75 31
150 98
220 137
240 131
260 115
240 98
220 81
150 52
75 42
30 80

Corrective Action
Often there is no alternate device and package available when warpage is identified as a root cause of HnP. In those cases, a
common corrective action is to modify the stencil printing to provide additional paste volume to bridge the gap (illustrated in
Figure 6) at the potential HnP sites [6]. Such a recommendation for the 144 I/O FBGA is shown in Figure 7. This stencil
recommendation was provided by the device supplier and was based on extensive Moiré studies of warpage in the 144 I/O
FBGA package. Implementation of this stencil modification improved the manufacturing yields from approximately 10% to
80% but did not eliminate the HnP defects entirely. The stencil modification also introduced some solder bridge (short circuit
condition) defects, which is an expected consequence of increasing paste volume with a fine pitch device.

A comparison of the stencil modification and the defect maps shown in the lower part of Figure 7 indicate that the increased
paste volume will mitigate the HnP problem in only about 75% of the FBGA sites used in this telecommunications
application (Note that these diagrams show the same package layout as those in Figure 4 and 5 but here they are viewed from
above to coincide with the stencil pattern.). This result is consistent with both the yield improvement and with the
observation that HnP defects were not eliminated completely. Despite the vast improvement, an 80% yield is unacceptably
low. However, given the demonstrated ambiguity in all aspects of the HnP defect characterization, it is more critical to
recognize that the 80% distribution may contain latent defects that can “escape” into service. In the absence of a definitive
non-destructive detection technique, this produces an unknown risk in subsequent field failures.

Figures 7. Proposed stencil modifications and effectiveness in mitigating HnP defects in the telecommunication Case Study
2 application of the 144 I/O FBGA package.
Summary – Limitations in Mitigating HnP though Paste Printing Modifications
Case Study 1 for a 144 I/O, 0.8 mm pitch FBGA shows that HnP defects are not limited to Pb-free assembly and can occur
with a typical SnPb soldering profile. Detailed root cause analysis shows that stencil printing modifications that provide
additional paste volume at the potential HnP sites can be used to bridge the gap during reflow and minimize HnP defects.
However, the effectiveness of printing modifications will depend on the magnitude and extent of the relative warpage
between the BGA component and the PCB. The specific application of a 144 I/O FBGA presented here possibly represents a
worse case scenario, in which yields will be defined by a tradeoff between bridging and effective soldering resulting from
additional solder volume. These results indicate that the characterization of the 144 I/O FBGA HnP and corrective action
described here can not be translated directly to other applications of the 144 I/O FBGA without incurring risk.

CASE STUDY 2 – 484 I/O PBGA


Problem Description
In this application, a 19mm x 19mm. 0.8 mm pitch, 484 I/O PBGA component exhibited variable or erratic production yields
when used in a complex telecommunication printed circuit board assembly (PCBA). The PCBA contained an array of
multiple SnPb 484 I/O PBGA (Figure 8) components. Only some of the sites had HnP defects, the frequency of defects
varied dramatically from one PCBA to another, and the overall yield was approximately 80%. Defects were mostly localized
at the corners and in the outer rows of the BGA but each component location and PCBA had a unique pattern or number of
HnP defects. Optical inspection images of HnP defects are shown in Figure 9. Data provided by the device supplier indicated
that this component was susceptible to warpage but was less sensitive to HnP defects when used in high temperature, Pb-free
solder assembly process.

Figure 8. The 484 I/O PBGA pin diagram.

Figure 9. Optical images of multiple HnP defects in a single 484 I/O PBGA.

Multiple sets of detailed photomicrographs of HnP defects in the 484 I/O PBGA are shown in Figures 10-12. Collectively,
these photomicrographs illustrate the scope of the HnP problem with the 484 I/O PBGA used in this telecommunication
application, as well as the subtle and insidious latent character of HnP defects. The photomicrographs in Figure 10 show an
HnP defect that will likely fail electrical testing due to the gap that exists at the interface between the solder ball and paste
after resolidification. The photomicrographs in Figure 11 show an HnP defect that is very likely to pass electrical testing and
may pass thermal screening and escape detection, only to fail after some undetermined time in service. The ball and paste in
this solder joint are making good mechanical contact, but the highest magnification images show that there is no continuity in
the solder microstructure across the interface. An argument could be made that a sub-microstructural, diffusion bond exists
between the two masses of solder but there clearly has been no actual solder coalescence and solidification across the
interface. The photomicrographs in Figure 12 show an HnP defect that will pass all routine factory testing. The ball and paste
in this solder joint are connected across only about 30-40% of the area of a normal, well-formed solder. There are no existing
data that could be used to predict the risk of failure for this solder joint in service.

Figure 10. A series of optical photomicrographs of an HnP defect in the 484 I/O PBGA. This HnP defect is likely to be
detected in electrical testing in the factory due to the gap between the solder ball and paste following reflow and
resolidification.

Figure 11. A series of optical and scanning electron micrographs of an HnP defect in the 484 I/O PBGA. This HnP defect
may not be detected in the factory due to the good mechanical contact at the HnP interface between the solder ball and paste.
Figure 12. A series of photomicrographs of a HnP defect in the 484 I/O PBGA that will pass all routine factory testing. The
ball and paste in this solder joint are connected across about 30-40% of the area of a normal, well-formed solder. The risk of
failure of this latent defect cannot be quantified.

Root Cause Analysis


Based on the characteristics of the yield data, the initial focus of the root cause analysis was on package coplanarity or
warpage. The most common technique for characterizing the extent of the warpage is by performing a Shadow Moiré scan
[7]. Shadow Moiré scans can detect surface deviations dynamically using a simulated surface mount reflow profile at specific
temperature read points of interest. The Shadow Moiré scans from one of the devices from the initial set are show in Figure
13. The scans simulate a reflow profile by starting at room temperature, peaking at 230º C and then returning to room
temperature.

The results of the Moiré testing indicate significant package warpage occurs throughout the reflow process temperature range.
Table 2 summarizes the Moiré results for four devices, showing the initial coplanarity measurements, peak coplanarity
measurements, and the total variation through the reflow temperature range. The data in this table show there is a maximum
coplanarity or warpage of 200.7 microns (7.9 mils) during the reflow process. Four additional devices were sent to the
packaging house for independent confirmation of the Moiré measurements. Those results are summarized in Figure 14 and
show a maximum warpage as great as 219.0 microns (8.6 mils) with a deviation from flatness of approximately 75 microns
( 3 mils) at SnPb liquidus. The second set of data provides confirmation of the findings from the initial set of measurements
shown in Table 2. These Moiré data show similar trends as the 144 I/O FBGA discussed in Case Study 1.The warpage is not
symmetric around the peak temperature and is not completely reversible or recoverable following the simulated reflow
temperature cycling.
Figure 13. Example of a Shadow Moiré output scans for a 484 I/O PBGA.

Table 2. Summary of Shadow Moiré results for 4 different 484 I/O PBGA components.
Device Initial Co-planarity Peak Co-planarity Total Variation
Number μm (microns) μm (microns) μm (microns)
1 91.4 @ (22ºC) 68.6 @ (230ºC) 160.0
2 104.1 @ (22ºC) 83.8 @ (180ºC) 188.0
3 99.1 @ (22ºC) 58.4 @ (210ºC) 157.5
4 96.5 @ (200ºC) 104.1@ (90ºC) 200.7
Figure 14. Summary of the Shadow Moiré testing of four additional 484 I/O, 0.8 mm pitch PBGA components performed
independently at the packaging house.

The Shadow Moiré warpage results for the 484 I/O PBGA show that the maximum deviation in package flatness occurs in
the SnPb reflow range above 183º C. Discussions with the device supplier revealed that a major change in the package mold
compound had been made to accommodate the brittle properties of the device 90 nm low-K dielectric. Working in
conjunction with the device supplier, Shadow Moiré was performed on two older generations of the device that used a
different mold compound. The Moiré results showed that the component with the newer mold compound warped
approximately 40% more than the older generation component.

In summary, the Moiré measurements and device supplier data show there is a certain amount of warpage inherent in the 484
I/O PBGA components. The warpage can not be eliminated and it can vary significantly from component to component. In
the worse case interactions with localized PCB warpage, this can result in HnP defects. In view of the package constraints,
mitigation of those defects must be focused on surface mount assembly process modifications or controls.

Stencil Design, Solder Paste Selection and Paste Printing


The art of stencil printing has become a very complex operation due to the extreme mix of component technologies used in
complex telecommunication designs. These components include micro-discrete resistors and capacitors, super-large discretes,
large plastic and ceramic area arrays, 0.4 mm pitch QFP and TSOP, 0.5 mm pitch QFN, and large power supplies and
transformers. To handle these components, varying volumes and heights of solder paste are needed, which makes stencil
design an important factor in the Design For Manufacturability (DFM) reviews. The use of 5 mil stencils has become
common with most contract manufacturers, which may satisfy IPC-610D inspection criteria but may not be sufficient to
avoid HnP defects. One other important factor to consider is variation in solder paste properties and performance from
manufacturer to manufacturer. Some solder pastes in fact, are advertised as being capable of mitigating HnP defects. Good,
consistent print quality, which is required to mitigate HnP risks, is a challenge considering the need to balance all the
potential design and manufacturing constraints.

A two-phase solder process analysis was conducted as a result of the outcome of the preliminary root cause warpage analysis.
The first phase was a Design of Experiment (DOE) to evaluate solder paste printing and the second phase was an evaluation
of the impact of solder printing on assembly and propensity for HnP. The DOE developed specifically to examine the solder
paste printing performance used the normal line output as the baseline metric. Automated 100% Solder Paste Inspection (SPI)
was done for six different commercial solder pastes with the DOE being focused specifically on the 484 I/O PBGA devices.
The paste printing DOE consisted of 30 printed boards of each paste and generated scatter plots for area, height, and volume.
Following the printing DOE an assembly DOE was run to assess the ultimate performance of the paste printing. Figure 15
shows the scatter plots for the paste printing DOE.

The scatter plots show that paste D clearly had the tightest, most consistent variations in area, height, and volume. Pastes A,
C, and F had some aperture clogging and required additional cleaning. These data were used to select the pastes for the
assembly phase of the study. Paste C was eliminated based on poor performance and paste E was eliminated due to
availability. Despite poor print performance, pastes A and F remained in the assembly phase matrix because both pastes have
advertised effectiveness for eliminating HnP defects. The effectiveness of these pastes is based on their prolonged flux
activity, which promotes wetting and soldering better during the ramp down [4]. Thus, solder pastes A, B, D, and F were
chosen for the final assembly evaluation phase.

Figure 15. DOE scatter plots for solder paste area (top), b) height (middle), and c) volume (bottom). Solder paste “D” in
blue was the best performer with the lowest variations in area, height, and volume.

The sample size for the assembly matrix was 50 each for pastes A, B, and F and 70 each for D. The yield results are showed
in Table 3. In the SMT operations, paste A performed well despite its poor performance in the paste DOE. Paste D showed
poor results in the SMT operations due to shorts. It appears that the added volume of solder paste resulted in increased shorts,
which is a common over-correction when dealing with HnP. Although the assembly yield for paste D was lower than the
other pastes because of solder shorts, from a product reliability standpoint paste D had the best results in the thermal test
indicating that there would be fewer escapes related to HnP defects with paste D than the other pastes. This is an important
finding because it indicates that a product risk analysis should be conducted to determine if a lower assembly overall yield
actually provides better product reliability and a lower life cycle cost. In simplest terms, this is reduced to a tradeoff between
solder shorts that can be detected and corrected in the factory and HnP defects that may escape manufacturing, reduce
reliability, and increase life cycle cost.

Table 4 shows the defects associated with the 484 I/O devices as a function of assembly operation. There were no visible
defects identified during SMT. The 5DX (X-ray) operation was unable to detect HnP but it did detect one short each with
pastes B and D. These two defects were associated with the increase in solder volume due to the increase in solder height and
area. For the In Circuit Testing (ICT), Functional Testing and Thermal Screening Testing operations, the 484 I/O device
failures were inspected using a BGA video microscope to confirm the HnP defects. All the failures detected during ICT,
Functional Test, and Thermal testing for devices assembled with pastes A, B, and F were confirmed as HnP defects. The
Thermal Test failure for paste D was not confirmed as an HnP on the outer perimeter and X-ray inspection did not detect HnP
in the inner rows. The device was immediately re-reflowed but it continued to fail. and it was presumed to be a device failure.
Since paste D had the most consistent results in the print DOE and showed the best performance for mitigating HnP defects
in the assembly testing, it was considered the best candidate for corrective action.

The data from the two-phase DOE showed that a carefully chosen combination of paste selection and print control could
provide significant mitigation of HnP defects. When solder paste D was implemented into the production process, it was done
in conjunction with incorporation of 100% solder paste inspection (SPI) to enable improved manufacturing process control.
The SPI was viewed as a critical step because it was needed to maintain control of a soldering process with a relatively
narrow window for success. By all accounts, it seems that deviation from the optimum process window results in
unacceptable levels of HnP defects in the 484 I/O devices. The corrective action plan required process changes and quality
monitoring that deviated from conventional manufacturing practices. Those process changes required substantial resource
commitments in manufacturer but this eliminated nearly all HnP defect, and resulted in acceptable production yields.

A few brief reflow trials showed that the reflow profile did not have as much of an impact as might be expected. This may
not be true for all cases of HnP, but the 484 I/O devices tended to have serious warpage in the 150-200º C range and had
minimal additional warpage up to 260º C. Therefore, minor profile adjustments had no measureable effect on the incidence of
HnP. The profiles used for the assembly DOE were adjusted to align with the profile parameters recommended by paste
manufacturers.
Table 3. Overall assembly results for pastes A, B, D, & F.
Operation B D F A
SMT
Bottom 80.00% 85.51% 84.00% 98.00%
SMT Top 84.00% 42.03% 84.00% 92.00%
5DX 86.00% 75.38% 88.00% 88.00%
ICT 86.00% 82.81% 85.71% 86.00%
Functional
Test 100.00% 100.00% 100.00% 100.00%
Thermal
Test 89.19% 93.44% 87.88% 81.25%

Table 4. 484 I/O PBGA device defects. Paste D was selected for process corrective action
Operation B D F A
SMT
Bottom 0 0 0 0
SMT Top 0 0 0 0
5DX 1 1 0 0
ICT 4 0 1 10
Functional
Test 1 0 2 3
Thermal
Test 5 1 1 0

Summary – Mitigating HnP by Controlling the Manufacturing Processes


The analysis for Case Study 2 for a 484 I/O, 0.8 mm pitch PBGA shows that it may be possible to control the onset of HnP
defects caused by component warpage through extraordinary manufacturing process controls. In this case, a combination of
solder paste selection, stencil print modifications, enhanced inspection techniques, and diligent monitoring of all the
processes provided the only practical path for corrective action. It can not be emphasized enough that it was critical to
develop good process methods and continue to monitor their effectiveness in practice.

CASE STUDY 3 – BGA HnP in New Product Introduction (NPI)


Problem Description
In this application various complex telecommunications Pb-free development products exhibit intermittent or open FBGA
and PBGA component solder joints. The rapid expansion of 3G and 4G telecommunications has dramatically changed New
Product Introduction (NPI). Design cycles have been reduced from years to months, and multiple designs are being
developed simultaneously to meet customer demands for features and performance. The combination of high-mix, low-
volume, product diversity, and aggressive schedules is causing an increased occurrence of HnP and intermittent BGA solder
joint defects in NPI. Figure 16 shows two examples of new telecommunication products. The PCBA geometries are
considerably different and there is a wide range of BGA component sizes and pin counts being used as evidenced by the x-
ray images included in Figure 16.

Figure 16. Examples of variation and range of components seen in telecommunication NPI.

It is common for test coverage development to be incomplete in NPI. In many cases visual inspection and conventional x-ray
are the only inspection tools in use. However, interpretation of optical and x-ray images can be very operator dependent.
Figure 17 shows optical and x-ray images of corner sites on the 473 I/O PBGA from Figure 16. It is easy to see from these
images that the solder joint is “lumpy”. Without extensive root cause analysis, it was difficult to determine if the lumpiness
was due to inadequate reflow temperature, insufficient solder paste, or insufficient flux activity due to a poor or dried out
solder paste.

Similar to Case Studies 1 and 2, many of the solder joint defects appear to be located at corner or edges of packages. Note
that there may be defects at interior sites that can not be detected with simple visual, optical, or x-ray inspection. The high-
mix, low-volume start and start/stop mode of operation in an NPI environment is not conducive to acquiring statistical failure
information needed to identify the defect root cause. Figure 18 shows solder joint defects in a 473 I/O PBGA on another NPI
build. The defects on this board show not only HnP and insufficient solder joints but also no-solder defects. There is also a
misalignment of the BGA balls to the PCB pads. The no-solder defects may have been due to plugged stencil apertures and
the insufficient and HnP defects may have been due to poor release of solder paste from stencil apertures.
Figure 17. Lumpy solder joints on a 473 I/O 0.8mm pitch PBGA

Figure 18. 473 I/O PBGAs in another NPI build exhibit various defect signatures than those in Figure 17.

Figures 19 through 22 show HnP defects in 84 I/O FBGA and 64 I/O PBGAs on other NPI products. The HnP defect in
Figure 20 could be detected using a small 45 degree inspection mirror on the end of probe or by using a BGA video
inspection tool. An examination of the 84 I/O FBGA conventional 2D x-ray image in Figure 21, shows an apparent
difference between the A3 HnP defect and surrounding ball sites. However, without the optical image the x-ray image is not
sufficient to identify this solder joint anomaly as HnP. In fact, one would be hard pressed to determine from the x-ray image
that this was a defective solder joint site.
Figure 19. HnP defect on 84 I/O SDRAM FBGA. The optical inspection system or microscope and mirror may be useful for
a BGA not near the PCBA edge but these are difficult to use, have marginal image quality, and require operator skill and
experience.

Figure 20. The HnP defect on the 84 I/O SDRAM FBGA is difficult to detect with x-ray inspection.

The conventional 2D x-ray image of defects on a 64 I/O PBGA presented in Figure 21 can not identify HnP or insufficient
solder joints. In the absence of the optical inspection images shown in Figure 22, it would be impossible to determine that
these sites had HnP and insufficient solder joint.
Figure 21. Conventional 2D x-ray imaging is not adequate for detecting HnP or insufficient solder defects.

Figure 22. Optical inspection images of outer edges of BGAs is a time-consuming process but it may be necessary to detect
HnP or insufficient solder defects.

Root Cause Analysis


Although the defects seen in Case Study 3 are at or near the outside edge of packages, the different types of defects including
lumpy joints, HnP, insufficient and no-solder defects suggest that there are quality and process problems in addition to
package warpage. Although some of the HnP intermittent solder joint defects were detected during visual inspect after an
NPI build, functional testing of other boards during Design Verification Testing (DVT) revealed intermittent solder joints on
boards that passed optical inspection. The incurred cost of these product assemblies and the customer demands prohibited the
type of destructive physical analysis that was done in Case Studies 1 and 2. A few of the defective NPI boards were re-
flowed using a BGA repair station and a few were re-reflowed using the original SMT assembly process in an attempt to fix
the intermittent solder joints. The additional heating cycles seemed to help on some boards but they did not correct all the
intermittent defects. It is important to note that even some that appeared to be corrected again failed during subsequent DVT.

In an effort to determine the root cause for the intermittent and HnP defects, a detailed review of the assembly process and
operations was conducted. This review determined that while package and board warpage was certainly a major contributing
factor to HnP defects, the situation was exacerbated by insufficient attention to the up-front assembly process, specifically
solder paste and stencil printing. Many of the automatic inspection features of stencil printing machines were not being used
and inspection of solder paste prints for area array packages was only being conducted on the initial board processed. More
importantly, it was found that solder paste time on a stencil was not being monitored and the practice of not recording the re-
use of solder paste was not only causing poor release of solder paste from stencil apertures but also the partially dried out
paste was reducing the fluxing action during reflow.

Corrective Action
The initial corrective action was to increase the solder paste volume by using a thicker stencil. What at first appeared to be an
easy and obvious corrective action for insufficient and HnP defects, actually resulted in increased frequency of defects. The
real mitigation for insufficient and HnP solder joint defects in this NPI assembly was to insure that the correct amount of a
“good” solder paste was applied to each area array package footprint. This entailed monitoring solder paste out-of-jar
exposure time, using more of the stencil printer automatic inspection features, and manually inspecting solder paste prints on
all area array footprints. Utilization of a solder paste specifically formulated to address HnP defects and laser cut and
electroformed stencils instead of chemically etched stencils also proved helpful in mitigating insufficient and HnP defects.
Increasing stencil apertures helped release of solder paste and increased solder paste volume but also increased the
occurrence of solder bridges. From a solder assembly process perspective, the root cause of the HnP defect was the result of
the sum of all the component and assembly process tolerances.

Summary – Mitigating HnP in NPI Environment


The lessons from Case Studies 1 and 2 have shown that component tolerance issues are an important factor in HnP defects
and the results from Case Study 3 have shown that stricter assembly process controls may be required. It is important to
recognize that conventional or historical specifications and guidelines may not be sufficient to prevent solder defects such as
HnP within the constraints of the current design and manufacturing environments.

DISCUSSION
Root Cause of HnP
There are several factors that can contribute to the HnP phenomena including package co-planarity, package warpage, PCB
warpage, and assembly issues associated with solder paste characteristics and stencil printing. There would be far less
incidents of HnP if package warpage was eliminated completely but of course, that is not practical. Furthermore, BGA
package warpage and coplanarity issues have existed since the advent of non-ceramic substrates [5]. While the case studies
presented in this paper certainly suggest that warpage is a major contributor to HnP, they also show that the HnP root cause
often results from a build-up of all of the component, printed circuit board, and assembly process tolerances. Tolerance build-
up can in fact, lead to HnP with packages that meet nominal package warpage specifications.

In an indirect way, the ongoing conversion to Pb-free manufacturing may be partly responsible for the increase in HnP
defects. Over the past 5 years, device suppliers and packaging houses have been modifying their offerings in preparation for
compatibility with high temperature, Pb-free assembly processes. As a result, most of the current BGA package offerings
exist in SnPb and Pb-free versions, with the only physical difference being the solder ball composition. However, these
packages must now perform adequately for both SnPb and Pb-free soldering applications, which includes a significantly
larger temperature range than the SnPb process alone. These case studies show that HnP defects are not limited to Pb-free
assembly and can occur with typical SnPb solder assembly. Furthermore, some of the warpage data indicate that
performance may be adequate for one reflow range but not the other (SnPb vs. Pb-free).

Industry Standards
There are two major industry standards for package warpage, the JEDEC, U.S. Standards [8-10] and JEITA, Japanese
Standard [11]. The JEITA standard has the tighter tolerances and many devices, including several discussed here, fail to meet
this standard. At the same time many of these devices that met the JEDEC standards exhibited HnP assembly defects in
production. This would imply that the JEDEC standards do not sufficiently account for the end-point manufacturing
requirements and constraints. This can create awkward situations in terms of corrective action when the warpage is indicted
as the root cause of HnP but the industry standard does not support that conclusion.
Inspection and Detection of HnP
Detection of HnP defects is challenging, even when they are located in the outer, more accessible rows. There is no doubt
that BGA video cameras and other optical or visual methods can detect HnP and sophisticated 5DX X-ray systems can detect
some but not all HnP defects. The problem is that the manner in which that these methods are used in routine factory
inspections is likely to find the HnP defects. These methods are best at finding defects when they are used as custom
inspection tools, which requires skilled operators and is not compatible with high speed production.

Rework or Repair of HnP


When an open circuit BGA failure is detected, there may be an attempt to correct the problem by re-reflowing the BGA
solder joints using either the SMT line or a BGA repair station. Reflow or repair methods were applied to the HnP defects in
Case Study 3 and the results were mostly unacceptable. This should not come as a surprise, since same warpage that caused
the original defect again will come into play during subsequent reflows. Another major reason that HnP rework is
undependable is because “HnP” is not a single defect mode but rather a spectrum of solder defects as illustrated in Figures
10-12. In Case Study 3, some of those defect structures responded positively to re-melting, while others continued to fail.
Even more importantly, some that appeared to be corrected initially again failed during subsequent testing. The real concern
is that re-reflowing may only “stick” these interfaces together without forming a true solder joint as shown in Figure 10.
These latent defects can escape manufacturing and fail in service. For this reason, these repair operations are considered high
reliability risks and are not recommended even if the defect population is fairly well-characterized.

CONCLUSIONS AND RECOMMENDATIONS


The conclusions and recommendations from the HnP defect analyses for the three telecommunications Case Studies are as
follows:
ƒ BGA package warpage is a major contributor to HnP defects, but HnP can occur when almost any of the assembly
process parameters deviate from acceptable practices. Often tolerance build-up of all the process parameters leads to
HnP defects. This can happen even in cases where package performance is consistent with existing industry warpage
specifications.
ƒ HnP defects are not limited to Pb-free assembly and can occur with typical SnPb solder assembly.
ƒ If a device or package exhibits HnP due to peak warpage at SnPb soldering temperatures, it may not necessarily exhibit
susceptibility to HnP defects when used at higher, Pb-free soldering temperatures.
ƒ Stencil printing modifications that provide additional paste volume at the potential HnP sites can be used to bridge the
gap during reflow and minimize HnP. This is not a foolproof technique; its effectiveness will depend on the magnitude
and extent of the relative warpage between the BGA component and the PCB. The specific application shown here of
the 144 I/O FBGA may represent a worse case scenario, in which yields will be defined by a tradeoff between bridging
and effective soldering resulting from additional solder volume.
ƒ Together, these results show that the root cause analysis and characterization of a specific case of HnP and
recommended corrective action may not be appropriate for other applications of the same BGA package. It is
recommended that specific empirically-based guidance be developed for each case of HnP, and each combination of
BGA and PCBA design.
ƒ Routine factory BGA inspection systems and electrical test methods can not be expected to detect, screen or eliminate
all HnP defects.
ƒ Adherence to conventional specifications and guidelines may not be sufficient to prevent HnP solder defects within the
constraints of the current design and manufacturing environments. When package warpage is the primary cause of HnP,
the only practical corrective action available to manufacturing is to develop custom assembly processes and methods
and diligently monitor their effectiveness in practice.
ƒ Case Study 2 showed that the SPI (solder process inspection) and additional quality monitoring that exceeded
conventional manufacturing practices were critical in order to maintain control and enable success over a relatively
narrow window. Deviation from this narrow, custom process window caused the HnP defects.
ƒ Correcting HnP defects by re-reflowing (re-melting) is considered a high reliability risk and is not recommended.
ƒ Industry standards organizations could ameliorate the HnP situation by scrutinizing the cause and effect relationship
between package warpage and HnP and by developing guidelines that would drive improvements in package warpage
performance. Process modifications can mitigate HnP defects but may not eliminate defects or “escapes.” Additionally,
these mitigation practices tend to shrink process windows, and make overall process control more difficult and costly.
Even moderate increases in defect and field return rates can be devastating in today’s cost-conscious environment. The
preferred corrective action is to minimize warpage to the extent that extraordinary process modifications and controls
can be avoided.

ACKNOWLEDGMENTS
The authors want to thank Andy Giamis of the Andrew Corporation for his technical contributions. They also want to
recognize the management support of this work from Marc Benowitz, Sherwin Kahn, Walter Nemes, and Wayne Tylka of
Alcatel-Lucent and Iris Artaki of the Andrew Division of CommScope.

REFERENCES
[1] Dudi Amir, Raiyo Aspandiar, Scott Buttars, Wei Wei Chin, and Paramjeet Gill, “Head – and – Pillow SMT Failure
Modes,” Proceedings SMTAI, 409-421, San Diego, CA, (2009).

[2 Masato Shimamura, Tetsuya Okuno, Satoru Akita, and Derek Daily, “Awakening from Head-in-Pillow: A Novel Pre-
Production Test Method fro BGANon-Wet Issues,” Proceedings SMTAI, 422-429, San Diego, CA, (2009).

[3] Li Li, Ken Hubbard and Jie Xue, “Improving Board Assembly Yield through PBGA Warpage Reduction,” Proceedings
ECTC 2009, 949-953, San Diego, CA, (2009).

[4] Jasbir Bath, Roberto Garcia, Noriyoshi Uchida, Hajime Takahashi, Gordon Clark, and Manabu Itoh, “Investigation and
Development of Tin-Lead and Lead-Free Solder Pastes to Reduce the Head-in-Pillow Component Soldering Defect,”
Proceedings SMTAI, 430-437, San Diego, CA, (2009).

[5] R. Lathrop, “BGA Coplanarity Reduction during the Ball Attach Process,” Proceedings SMTA Pan Pacific Conference,
2008.

[6] Mradul Mehrotra, Stephen R. Stegura, John R. Campbell, Martin L. Scionti, Emmanuel J. Siméus, and Javier E. Enriquez,
“BGA Warpage and Assembly Challenges,” Proceedings SMTAI, 297-308, Chicago, IL, (2004).

[7] V. J. Parks, “Geometric Moiré,” in Handbook on Experimental Mechanics, A. S. Kobayashi, Ed.Englewood Cliffs, NJ,
Prentice-Hall, 282-313.

[8] JESD22-B112, “High Temperature Package Warpage Measurement Methodology,” JEDEC Solid State Technology
Association, 2005.

[9] JESD22-B108A, “Coplanarity Test for Surface-Mount Semiconductor Devices,” JEDEC Solid State Technology
Association, 2003.

[10] JEDEC Publication 95, SPP-024 Issue A, “Reflow Flatness Requirements for Ball Grid Array Packages,” JEDEC Solid
State Technology Association, 2009.

[11] JEITA, JEITA ED-7326, “Measurements Methods of Package Warpage at Elevated Temperature and the Maximum
Permissible Warpage,” Japan Electronics and Information Technology Industries Association, 2007.
Telecommunications Case Studies
Address Head-in-Pillow (HnP) Defects and
Mitigation through Assembly Process
Modifications and Control

Russell Nowland1, Richard Coyle1,


George Wenger2, and Peter Read1

1Alcatel-Lucent, 2Andrew Division of CommScope

1
OUTLINE

ƒ Background Information
ƒ Head-in-Pillow (HnP) Defect Formation
ƒ 3 Case Studies of HnP (144 I/O FBGA, 484 I/O PBGA,
multiple BGAs in NPI)
ƒ Problem statement
ƒ Root cause Analysis
ƒ Corrective action or mitigation
ƒ Discussion
ƒ Conclusions and Recommendations

2
HEAD-in-PILLOW (HnP) DESCRIPTION

ƒ Evolving package and PCB technologies have resulted in


an increase in an open or intermittent ball grid array (BGA)
defect called head-in-pillow (also called head-on-pillow,
head and pillow, ball-in-cup, ball and socket).
ƒ Head-in-Pillow (HnP) is characterized by complete
melting of both the solder paste and the BGA solder ball
but with insufficient coalescence to produce well-formed
solder joints.

3
The solder ball and paste melted but did not coalesce.
HEAD-in-PILLOW DEFECT MECHANISM
ƒ HnP defects are created when a gap develops between the
ball and the solder paste during the reflow process due to
dynamic warpage of the package or PCB. Insufficient flux
activity on the surface of the ball or contamination on the
solder ball or molten solder paste prevents coalescence.

4
from Amir et al (Intel), SMTAI 2009
CASE STUDY 1
144 I/O FINE PITCH BGA (FBGA)
Problem Description
ƒ Multiple SnPb 144 I/O 0.8 mm pitch FBGA components are soldered onto
a large telecom PCBA
ƒ Each BGA location on the PCBA has a unique occurrence frequency and
pattern of HnP defects.
ƒ Device supplier data indicated that component was not sensitive to HnP
defects when used in a Pb-free solder assembly process.

5
CASE STUDY 1
144 I/O FINE PITCH BGA (FBGA)

BGA #1
Defect map

6
CASE STUDY 1
144 I/O FINE PITCH BGA (FBGA)

BGA #2
Defect map

ƒ Variations in HnP appearance.

ƒ Defects not limited to the corners or edges of the package. 7


CASE STUDY 1
144 I/O FINE PITCH BGA (FBGA)

This is an insidious type of HnP defect because it can


BGA #1 U11 escape manufacturing and result in an early failure.

8
CASE STUDY 1
144 I/O FINE PITCH BGA (FBGA)

Observations Moiré Data


Temperature Warpage
ƒ Identical devices have very differently
HnP signatures when assembled onto °C µm
two different locations of the PCBA. 30 70
75 31
ƒ Defects are not limited to the corners
or edges of the packages, the number 150 98
of defects varies by PCBA location, 220 137
and the defect patterns are not
symmetric for the two packages. 240 131
260 115
ƒ The HnP problem is not limited to Pb 240 98
free assembly. Peak warpage occurs
at SnPb peak temperature 220 81
150 52
75 42
30 80 9
CASE STUDY 1
144 I/O FINE PITCH BGA (FBGA)
Corrective Action

ƒ There are limitations to mitigating HnP though paste printing.


ƒ Note: This modification proved successful in some applications 10
of the 144 I/O FBGA.
CASE STUDY 2
484 I/O 0.8 mm Pitch Plastic Ball Grid Array (PBGA)
Problem Description
ƒ The SnPb PBGA exhibited erratic production yields when used in a complex
telecommunication PCBA. The PCBA contained an array of multiple
components. Only some of the sites had HnP defects, the frequency of defects
varied dramatically from one PCBA to another, and the overall yield was
approximately 80%. Defects were mostly localized at the corners and in the
outer rows of the BGA but each component location and PCBA had a unique
pattern or number of HnP defects.

11
CASE STUDY 2
484 I/O 0.8 mm Pitch Plastic Ball Grid Array (PBGA)
Three Different Types of HnP

Open - Immediate failure

Soldered – Possible long


term reliability risk

12
Contacting – Early failure risk (cold solder joint)
CASE STUDY 2
484 I/O 0.8 mm Pitch Plastic Ball Grid Array (PBGA)
Three Different Types of HnP
Root Cause Analysis

ƒ Peak warpage occurs in the critical range of SnPb reflow

Summary of Shadow Moiré results for 4 different 484 I/O PBGA components.

Peak Warpage Total


Device Initial Warpage
µm (microns) Variation
Number µm (microns)
µm (microns)
1 91.4 @ (22ºC) 68.6 @ (230ºC) 160.0

2 104.1 @ (22ºC) 83.8 @ (180ºC) 188.0

3 99.1 @ (22ºC) 58.4 @ (210ºC) 157.5

4 96.5 @ (200ºC) 104.1@ (90ºC) 200.7


13
CASE STUDY 2
484 I/O 0.8 mm Pitch Plastic Ball Grid Array (PBGA)
Three Different Types of HnP
Root Cause Analysis – Warpage-Induced HnP Defects

HnP defects form


in this
temperature range

14
CASE STUDY 2
484 I/O 0.8 mm Pitch Plastic Ball Grid Array (PBGA)

A two-phase solder process analysis was


conducted based on the results of the
warpage analysis.

ƒPhase 1 – Conduct a DOE to evaluate


solder paste printing of 6 commercial solder
pastes.

ƒPhase 2 – Evaluate the relationship


between solder printing, assembly, and
propensity for HnP.

ƒ Solder paste “D” was the best performer


with the lowest variations in area, height, and
volume in Phase 1.
15
CASE STUDY 2
484 I/O 0.8 mm Pitch Plastic Ball Grid Array (PBGA)

ƒSolder paste “D” was the best performer with the highest overall
assembly yield and was selected for process corrective action
ƒThe comprehensive corrective action plan included solder paste selection,
stencil print modifications, enhanced inspection techniques, and diligent
monitoring of all the processes

Operation B D F A Operation B D F A
SMT SMT
Bottom 80.00% 85.51% 84.00% 98.00% Bottom 0 0 0 0
SMT Top 84.00% 42.03% 84.00% 92.00% SMT Top 0 0 0 0
5DX 86.00% 75.38% 88.00% 88.00% 5DX 1 1 0 0
ICT 86.00% 82.81% 85.71% 86.00% ICT 4 0 1 10
Functional 100.00 100.00 100.00 100.00 Functional
Test % % % % Test 1 0 2 3
Thermal Thermal
Test 89.19% 93.44% 87.88% 81.25% Test 5 1 1 0

Overall assembly results for 484 I/O PBGA


16
pastes A, B, D, & F. device defects
CASE STUDY 3
BGA HnP in New Product Introduction (NPI)
Problem Description
ƒ Design cycles have been reduced from years to months, and multiple designs are
being developed simultaneously to meet customer demands. The combination of
high-mix, low-volume, product diversity, and aggressive schedules is causing an
increased occurrence of HnP.

17
CASE STUDY 3
BGA HnP in New Product Introduction (NPI)

ƒVarious solder defects including insufficient and no-solder


defects, in addition to HnP suggest that there are quality and
process problems besides package warpage.

18
CASE STUDY 3
BGA HnP in New Product Introduction (NPI)

ƒHnP defects in 84 I/O SDRAM


ƒNote: HnP can not be identified with X-ray

19
CASE STUDY 3
BGA HnP in New Product Introduction (NPI)

ƒHnP defects in 64 I/O PBGA can not be identified with 2D X-ray


ƒTime-consuming manual optical inspection may be required

20
CASE STUDY 3
BGA HnP in NPI
Root Cause and Corrective Actions

ƒPackage and board warpage was a major contributing factor. HnP


was exacerbated by insufficient attention to the up-front assembly
process, specifically solder paste and stencil printing.
ƒHnP was reduced by insuring that the correct amount of a “good”
solder paste was applied to each area array package footprint. This
entailed monitoring solder paste out-of-jar exposure time, using the
stencil printer automatic inspection features, and manually
inspecting solder paste prints on all area array footprints.
ƒIncreased stencil apertures helped release of solder paste and
increased solder paste volume but also increased the occurrence of
solder bridges.
ƒHnP was reduced by utilizing solder paste specifically formulated
to address HnP defects and laser cut and electroformed stencils
instead of chemically etched stencils.
ƒFrom an assembly process perspective, the root cause of HnP was the
21
result of the sum of all the component and assembly process tolerances.
CONCLUSIONS and RECOMMENDATIONS
ƒBGA package warpage is a major contributor to HnP defects. Tolerance
build-up of all the process parameters also leads to HnP defects, even in
cases where package performance is consistent with industry warpage
specifications.
ƒWhen package warpage is the primary cause of HnP, the only practical
corrective action available to manufacturing is to develop custom
assembly processes and methods and diligently monitor their
effectiveness in practice.
ƒStencil printing modifications can be used to bridge the gap during reflow
and minimize HnP. Process modifications can mitigate HnP defects but
may not eliminate defects or “escapes.” Additionally, these mitigation
practices tend to shrink process windows, and make overall process
control more difficult and costly.
ƒThe root cause analysis and characterization of a specific case of HnP
and recommended corrective action may not be appropriate for other
applications of the same BGA package. It is recommended that specific
empirically-based guidance be developed for each case of HnP, and each
combination of BGA and PCBA design.

22
CONCLUSIONS and RECOMMENDATIONS

ƒHnP defects are not limited to Pb-free assembly and can occur with
typical SnPb solder assembly.
ƒRoutine factory BGA inspection systems and electrical test methods can
not be expected to detect, screen or eliminate all HnP defects.
ƒCorrecting HnP defects by re-reflowing (re-melting) is considered a high
reliability risk and is not recommended.
ƒIndustry standards organizations should work to reduce the incidence of
HnP by developing guidelines that would drive improvements in package
warpage performance.
ƒThe preferred corrective action is to minimize warpage to the extent that
extraordinary process modifications and controls can be avoided. In these
case studies, warpage was a major contributor to HnP defects but the
situation was exacerbated by insufficient attention to the up-front
assembly process, specifically solder paste and stencil printing.

23

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