Implementationof Lean Concepts Using Value Stream Mappingin Automotive Firm
Implementationof Lean Concepts Using Value Stream Mappingin Automotive Firm
1 Introduction
2 Case Study
This research was carried out in a leading automobile industry located in Pune, Maha-
rashtra, India. There are various shops formed in the company such as transaxle shop,
engine shop, paint shop, assembly shop, and research and development center. After
analyzing and discussing with respective shop head, engine shop was selected for the
research work. The company performs operations on four different engine parts of
an engine in an engine shop, viz. (1) engine head, (2) block head, (3) crankshaft, and
(4) camshaft. After collection of relevant data and discussing with the manager of an
engine shop, the most critical product, i.e., crankshaft, has been selected for the value
stream mapping. In this study, crankshaft of diesel engine has been studied, as the
particular car was having huge demand in the market. As the target for crankshafts
was 120 per shift, however on an average 80 per shift was achievable. Following is
the information about working structure of the company.
(1) Number of shifts—2
(2) Target—120 jobs/shift
(3) Available time—8 h/shift
Total available time per shift
(4) Take time
Total demand time per shift
8 × 60 × 60
120
240 s
Implementation of Lean Concepts Using Value Stream Mapping … 143
3 Literature Review
Belokar et al. [4] implemented VSM in the manufacturing unit of Malaysia. D54T
from front disk assembly was selected, because it did not meet daily target. Future
state map revealed the wastes and increased the productivity, thereby meeting daily
production target. In Hines and Rich [5] VSM was developed to collect and use group
of tools to help researchers and various organizations to find various wastes and find
better ways to eliminate it. Aziziand Manoharan [8] studied PCB assembly line to
implement lean techniques. The main objective of the paper was to reveal the factors
which affect the smart tag production. The SMED technique was implemented at
the insertion process that was bottleneck. SMED technique was successfully imple-
mented as the machine setup time in the insertion process was reduced from 145
to 54 s. Tyagi et al. [9] explored about concept of VSM to the product develop-
ment process (PDP) stresses on the importance of faster product development for the
right edge on the market. Paper was narrowed down to the concept of development
of product. Further research is to be done in the field of value stream mapping on
other process of an organization. Rosa et al. [10] explored to change current working
methods of the assembly line to avoid delays in future if the customer demand is
increased. Various VSM tools such as 5S, TPM, and Kaizen were used to eliminate
waste and other issues, which increased the productivity of the line by 41% [11–13].
4.1.1 Bottleneck
In crankshaft production line bottleneck was found at the oil-hole drilling operation.
The frequent breakdown of machine caused delay in the operation and subsequently
more WIPs. Tool life of the drills was 60 jobs. Hence, operator had to change the
drills twice in 1 shift, which approximately costs one hour in 1 shift.
144 A. Deokar et al.
It has been observed that improper sequence of operations has been affecting the
productivity of crankshaft line. Many times due to unavailability of operator, debur-
ring operation is done after oil-hole drilling which is to be done immediately after
milling operations. Instead, it is done as milling—oil-hole drilling—deburring. Due
to this issue, jobs had to travel to and fro causing more WIPs and inventory leading
to more lead time and affecting the overall production of crankshaft line. Similar
case was found at induction hardening.
4.1.3 WIP
Large amount of work in process (WIP) between the processes hinders the further
operation resulting in delays. Operations such as induction hardening, grinding, and
oil-hole drilling contribute large amount of WIPs as compared to other operations.
This is mainly because unavailability of worker at workplace, breakdowns, issues
with the manager, improper sequence of operations, and lack of planning.
Work ethics and culture of the production line have been affecting the production in
terms productivity and lead time. It has been observed that operators of the various
machines at crankshaft line do not follow certain work ethics such as tools which are
not kept on assigned place. Many times cleaning of machinery before starting the
operation is neglected by the operators.
Figure 1 shows the current state VSM of case company with seven operations and
processing lead time as 2237 seconds.
Induction hardening was done on two machines. Due to unavailability of the shank
hardening coil at first machine, all jobs had to travel around 50 meters distance to get
shank hardened at second machine. After discussing with the management, with the
help of manager and line supervisor, they agree to shut down one induction hardening
machine and to harden all parts of crankshaft on second machine. Hence, to reduce
the processing lead time, immediately after oil-hole drilling deburring operation, all
jobs were shifted to second machine (Alfing). As a result, the cycle time reduced
from 395 to 168 s. However, certain changes had to made in the Alfing machine
to harden all parts of crankshaft, which costs around 0.8 million to the company.
Grinding and key way milling operations were leaned with the jigs and fixture tools
(Fig. 1).
4.3 Results
Implementation of VSM tools on current state map had shown significant reduc-
tion in cycle time of operations such as drilling, induction hardening, and grinding.
Eliminating bottleneck from the crankshaft line was major reason in the reduction of
processing lead time. The prominent waste identified was bottleneck, due to bottle-
neck large amount of WIPs used to create in the process. In continuation to that idle
time for following machines were reduced thereby lead time improvised by imple-
menting VSM tools such as 5S, TPM which increases the productivity of crankshaft
line. Results showed reduction in processing lead time of 438 s. Successful imple-
146 A. Deokar et al.
mentation of the VSM tools resulted in the reduction of cycle time by 56, 227, and
155 s of oil-hole drilling, induction hardening, and grinding, respectively. Finally,
there was an increase in the productivity, on an average by 24 units. Figure 2 shows the
future state VSM of case company with reduced processing lead time 1899 seconds.
5 Conclusion
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