Ahmad (2023)
Ahmad (2023)
256 10.1007/s00170-017-0783-2
DOI
ORIGINAL ARTICLE
Received: 6 March 2017 / Accepted: 6 July 2017 / Published online: 10 August 2017
# Springer-Verlag London Ltd. 2017
1
Department of Industrial and Production Engineering,
Bangladesh University of Engineering and Technology, Dhaka
240 Int J Adv Manuf Technol (2018) 94:239–
1 Introduction 256
8 Carannante et al. [19] A comparative study of the UK and Foundry factory UK and Japan
Japanese
foundry industries in implementing TPM Steel company Jordan
9 Almeanazel [6] To measure OEE and improve OEE
by applying TPM
10 Wudhikarn [97] To develop the present OEE by overall Fiber cement roof Thailand
weighting manufacturing company
equipment effectiveness (OWEE) based
on existing implementation of TPM
11 Ahuja and Kumar [4] To investigate the contributions of successful Precision tube mills India
TPM
initiative to competitive manufacturing
12 Tsarouhas [91] To increase the productivity of machinery and improve t
240 Int J Adv Manuf Technol (2018) 94:239–
product by adopting TPM 256 industry especially
Food Greece
13 Eti et al. [23] To implement TPM as a strategy and improve in bakery products
the performance of machinery and suggestion Nigerian manufacturing Nigeria
for self-auditing and benchmarking industry
14 Chan et al. [20] To study the effectiveness and implementation of
the TPM program in the industry Electronics manufacturing Hong Kong
company
15 Ljungberg [65] To establish a norm based on stoppage of Volvo Car Corporation Sweden
machinery
in the TPM framework
Int J Adv Manuf Technol (2018) 94:239– 24
256
[28, 29, 45], a strategic weapon for continuous fishbone diagram, WWBLA work sheet, and an overview
improvement [64], to improve the overall equipment of the yarn manufacturing process. Section 3 gives an
efficiency (OEE). To the best our knowledge, there is no overview of the case company. Section 4 gives the
literature that focused on the ring frame section of a textile methodology under- taken in this research. Section 5
processing factory for TPM study. Thus, this paper presents results and discus- sion of findings. Finally,
contributes to the total productive maintenance and textile Section 6 concludes the paper.
literature as follows:
Performance rate
Units produced in the total shift time
¼ x 100 ð3Þ
Number of expected units to be produced
ð5Þ
3 Overview of the case company (ATML), a sister concern of Akij Group, in Bangladesh. The company
is now producing rotor-spun yarn by installing a rotor frame. At
This study was conducted in Akij Textile Mills Limited present, the production capacity of the ring and rotor spinning
24 Int J Adv Manuf Technol (2018) 94:239–
256
system is 25 and 12 tons per day, respectively. Currently, there are around 1200 people
working in the factory. The factory has an installed
capacity of 45,000 spindles in the ring spinning system.
The industry was de- signed to produce carded, combed,
compact, Siro, cotton- polyester (PC), and chief valued
cotton (CVC) yarns. Akij Group has apparel manufacturing
facilities with very strong backward integrated industries
of spinning, weaving, dyeing,
Int J Adv Manuf Technol (2018) 94:239– 24
256
Fig. 2 Flowchart of carded yarn Processing
production Input Material Output Material
Machinery
Conditioning
Packing Bags
finishing, and packaging. They are supplying quality frame. Significant losses were identified using Pareto
knitted and woven fabric across the world to famous analysis. The WWBLA work sheets helped to find out the
retailers in the fashion industry. Some famous clothing reasons be- hind those significant losses. Then, the
retailers like HnM, Tema, BF Asia, etc. are buying finished fishbone diagrams were constructed to illustrate the causes
fabric from Akij Group. Therefore, this study carried of the problem in a structured way. A Kaizen team was
practical significance to Akij Group to benefit all formed to train the oper- ators to improve their skills on
backward linkage operations. basic maintenance works such as cleaning of machine
parts, oiling, tightening, inspection, and basic routine
works. After the training program, OEE of the same ring
4 Research methodology frame section was calculated in the same ways followed
before the training program. Finally, results were compared
The study was carried out in the ring frame section of a to assess the improvement in OEE. The study framework
yarn manufacturing factory. The main goal of this research can be visualized in Fig. 6.
was to improve the OEE through TPM. To measure the
OEE, six major stoppage losses in the ring frame section 4.1 Initial status of stoppage losses and OEE
were exam- ined. Based on the measured major stoppage
losses, the OEE was calculated and the ring frame with the It is essential to get appropriate data on stoppage losses to
lowest OEE was selected for further study. Three tools, implement TPM. Often, organizations keep record of
namely Pareto analysis, WWBLA work sheet, and cause- repair time in the logbook. However, they do not give the
and-effect diagram, were used to analyze data on stoppage actual scenario of stoppage losses and their causes in most
losses and OEE of the ring of the
24 Int J Adv Manuf Technol (2018) 94:239–
256
Roving
unit
Ring
Aprons
Components of the system
are not in scale with one
another to enhance
illustration
Separator plate
Ring rail
were chosen randomly to get the actual scenario of the pro-
duction process. Here, each working day consists of eight
Traveler working hours (one shift) as shown in Table 2. Various
Ring cop exper- iments were performed in this research in order to
get a real
Fig. 3 Schematic diagram of the ring frame [66] Fig. 4 Defective ring cops
Pareto Chart
Data analysis by analytical WWBLA
tools
Fishbone
Diagram
Training program for
operators
Measurement of OEE
multiple causes with a single effect. Figure 8 illustrates the be stored before changeover of count or lot. DCP and TCP
WWBLA work sheet for idling and minor stoppage. The gears were changed due to the new order of higher count,
countermeasures taken are also shown in Fig. 8. Based on which was a managerial decision. The productivity of
WWBLA, a fishbone diagram was constructed for idling machin- ery, process waste percentage, and the quality of
and minor stoppage. yarn were also dependent on end breakage rate of the ring
The fishbone diagram for idling and minor stoppage frame. As noticed, higher RH enhanced the end breakage
loss is displayed in Fig. 9. Based on the influence of man, rate. Thus, proper control of RH was in place to reduce the
machine, materials, measures, management, and end breakage rate in the ring frame section.
environment, the rea- sons for idling and minor stoppage Figure 10 gives the WWBLA work sheet for the break-
were categorized. Operators were not concerned about the down losses. The countermeasures taken have been shown
time required to re- lease the ring cops from the machine. in the WWBLA. The fishbone diagram is presented in Fig.
The front roller was displaced, and bearing was broken due 11 that is constructed based on the WWBLA for
to overloading of the machine. Due to the generation of breakdown losses.
piles through the front roller, travelers have flown away. Figure 11 presents the fishbone diagram for breakdown
To avoid count and lot mix, countwise bobbin color should losses. The reasons are grouped based on the influence of
be fixed. Therefore, a sufficient amount of countwise man, machine, materials, and measures. DCP gear is
colored empty bobbins should broken
Int J Adv Manuf Technol (2018) 94:239– 25
256
Table 2 Different stoppage
losses in the selected ring frame Day Activity Losses Frequency Total loss (min)
due to lack of skills of operators. Since the connection be- status. Table 4 shows the summary
tween nuts and bolts were loose, the front roller and TCP
gear shaft were displaced. Also, V-belts were broken. Also,
wast- age was increased due to the generation of piles
through the front roller. In that case, proper measures were
taken to adjust the front roller position and TCP gear shaft.
1 2 3 4 5 6 7 8 9 10
A Running time per shift (min) 480 480 480 480 480 480 480 480 480 480
B Downtime per shift (min) 0 0 0 0 0 0 0 0 0 0
C Loading time per shift (A − B) (min) 480 480 480 480 480 480 480 480 480 480
D Stoppage losses per shift (min) 32 30 31 50 38 36 35 40 42.5 41
E Operating time per shift (C − D) (min) 448 450 449 430 442 444 445 432 437.5 439
Defective amount (number) 97 106 112 106 106 102 108 124 95 109
F Output per shift (number) 3416 3317 3393 3483 3443 3487 3314 3393 3493 3363
G Rate of quality products (%) 97.16 96.80 96.70 96.96 96.92 97.07 96.74 96.35 97.28 96.76
H Ideal cycle time (min) 0.11 0.11 0.11 0.11 0.11 0.11 0.11 0.11 0.11 0.11
I Actual cycle time (min) 0.13 0.13 0.12 0.12 0.12 0.12 0.13 0.13 0.12 0.13
J Actual processing time (I * F) (min) 430.76 418.27 417.34 424.93 420.05 428.90 420.88 427.86 419.16 424.07
K Operating speed rate (H/I * 100) (%) 86.52 86.52 88.70 89.43 89.43 88.70 85.91 86.52 90.92 86.52
L Net operating rate (J/E * 100) (%) 96.15 92.95 92.95 98.82 95.03 97.60 94.58 97.24 95.81 96.60
M Availability (E/C) * 100 (%) 93.33 93.75 93.54 89.58 92.08 92.50 92.71 91.67 91.15 91.46
N Performance efficiency (K * L * 100) (%) 83.19 80.42 82.45 88.37 84.99 85.68 81.25 84.13 87.11 83.58
OEE = M * N * G * 100 (%) 75.44 72.98 74.58 76.76 75.85 76.93 72.87 74.31 77.24 73.97
Average OEE (%) 75.09
stoppage, which is 82% of the total loss. The second Figure 14 shows the comparison of OEE, output ring
signif- icant loss is breakdown stoppage. Here, though the cops, defective ring cops, and production rate before and
percent- age of idling and the minor stoppage was after im- plementation of TPM. It is revealed that the OEE
increased from is increased from 75.09 to 86.02%. It is due to the
71.6 to 82%, the overall stoppage losses were reduced by reduction of stoppage losses and an increase of output ring
42.13%. cops. After the training program, operators became more
Figure 13 compares stoppage losses in two scenarios, concerned about production and small maintenance
namely before reducing stoppage losses and after reducing activities. As a result, the number of idle spindles was
stoppage losses. Before and after applying Kaizen, reduced, and output ring cops were in- creased by 11.36%.
stoppage losses were 375.5 and 217.5 min, respectively. The defective ring cops were reduced by 49.53% (from
The losses were reduced to 158 min for 10 days, 15.8 min 107 pieces to 56 pieces). It was due to countermeasures
per shift, and that were taken to reduce stoppage
47.4 min per day.
60
200
Time (minutes)
50
40
150 30
20
100 10
0
50
0
Idling and Breakdown Yield loss minorReducedSet-up and Defects in speedadjustmentprocess
stoppage
Major stoppage loss
Cumulative Percentage
25 Int J Adv Manuf Technol (2018) 94:239–
256
Verification
Verification
Verification
Verification
Why? Why? Why? Why?
Description of
1st factor for 2nd factor for 3rd factor for 4th factor for Countermeasure
phenomenon
phenomenon phenomenon phenomenon phenomenon
Size of
problem
83.0 mins /80
1.1 1.1 V-belts
hrs = Broken belts are
1. Main motor between machine
8.30 mins/ 8 replaced
is stopped pulley and motor
hrs = 8.30
mins loss per pulley are broken
shift
3. Front roller 3.1 3.1 Piles are 3.1.1 3.1.1 Displacement Position of front roller
Breakdown bearing is originated of front roller is adjusted
losses broken through
front roller
Man Machine
Breakage of V-belt
Unskilled operator
Displacement of TCP gear shaft
Breakdown
losses
Piles are originated through front roller Adjustment of TCP gear shaft
Materials Measures
losses of the machine. The operators were more concerned result of taking countermeasures, stoppage time was
about the machine performance. It is noticed that when end reduced from 375.5 to 217.5 min.
breakage occurred in any spindle, the concerned operator According to Table 6, OEE is increased to 86.02% from
pieced together the ends of yarn at the breaking point, and 75.09% after countermeasures were taken. At the same
there was less chance to create a defective ring cop. time, the number of idle spindles was reduced and the
After taking countermeasure (shown in the WWBLA number of output ring cops was increased.
work sheet, Figs. 8 and 10), the stoppage losses were During the research period, the authors involved in this
reduced to study did not notice any organized company policy for the
21.75 min, and consequently, defective ring cops were re- training of operators. The operators and maintenance staffs
duced to 54 pieces per shift. The output ring cops were in- of the textile factory lacked the fundamental theoretical
creased to 437 pieces per shift. knowledge to examine and reduce stoppage losses and to
As a result of the reduction of stoppage losses as well as evaluate the OEE. On-the-job and off-the-job training may
for the improvement of OEE and product quality, the assist in developing the skill of operators and maintenance
production rate was increased by 23.93%. After staffs [35, 82, 96].
countermeasures had been taken, the stoppage losses per In this study, the off-line training program was arranged
shift were reduced to to develop the skill of operators. One pillar of TPM,
21.75 min, and consequently, defective ring cops were re- namely Kaizen, was implemented to the ring frame
duced to 54 pieces as well as output ring cops were machine in the textile spinning factory. As a result of
increased to 3847 pieces. The WWBLA work sheet (Figs. applying Kaizen, the stoppage time was reduced
8 and 10) displays the countermeasures that were taken to considerably. Reduction of
reduce stop- page losses to the ring frame of the spinning
factory. As a
1 2 3 4 5 6 7 8 9 10
A Running time per shift (min) 480 480 480 480 480 480 480 480 480 480
B Downtime per shift (min) 0 0 0 0 0 0 0 0 0 0
C Loading time per shift (A − B) (min) 480 480 480 480 480 480 480 480 480 480
D Stoppage losses per shift (min) 21.2 15.6 25.5 20 30 21.4 25 20.8 23 15
E Operating time per shift (C − D) (min) 458.8 464.4 454.5 460 450 458.6 455 459.2 457 465
Defective amount (number) 64 65 52 61 51 48 53 50 45 49
F Output per shift (number) 3978 3775 3912 3865 3727 3685 3920 3798 3889 3919
G Rate of quality products (%) 98.39 98.28 98.67 98.42 98.63 98.70 98.68 98.68 98.84 98.75
H Ideal cycle time (min) 0.11 0.11 0.11 0.11 0.11 0.11 0.11 0.11 0.11 0.11
I Actual cycle time (min) 0.11 0.12 0.12 0.117 0.12 0.12 0.12 0.12 0.12 0.12
J Actual processing time (I * F) (min) 453.49 441.68 449.88 452.21 436.06 438.52 450.8 448.16 447.24 454.60
K Operating speed rate (H/I * 100) (%) 95.70 93.25 94.87 93.25 93.25 91.68 94.87 92.46 94.87 94.05
L Net operating rate (J/E * 100) (%) 98.84 95.11 98.98 98.31 96.90 95.62 99.08 97.60 97.86 97.76
M Availability (E/C) * 100 (%) 95.58 96.75 94.69 95.83 93.75 95.54 94.79 95.67 95.21 96.88
N Performance efficiency (K * L * 100) (%) 94.59 88.69 93.90 91.67 90.36 87.66 93.99 90.24 92.84 91.94
OEE = M * N * G * 100 (%) 88.90 84.33 87.73 86.46 83.55 82.66 87.89 85.19 87.37 87.96
Average OEE (%) 86.20
stoppage time, in turn, decreased throughput time and in- by the WWBLA (Figs. 8 and 10) work sheet, the root
creased machine performance. It is mentioned here that im- causes were identified, and corrective actions were taken.
plementation of the TPM strategy did not interfere with The reduc- tion of stoppage losses helped in decreasing the
sched- uled maintenance, rather it helped reduce the idle number of spindles, in the reduction of the defective
stoppage time losses and increased the productivity. It also bobbin, and in the increase of production. The key results
gave the opera- tors the opportunity to raise their skills on of the application of Kaizen were as follows:
fundamental back- ground on maintenance operations
relevant to the application of total productive maintenance. • The reduction of defective ring cops was 49.50%.
The stoppage time loss in the initial stage was 37.5 min • The increase of output ring cops was 11.36%.
per shift, whereas after implementation of TPM, it was • The production was increased by 23.93%.
reduced to • OEE was increased from 75.09 to 86.20%.
21.75 min per shift. After analyzing the causes of the
stoppage
140 70
120 60
Time (minutes)
100 50
80 40
60 30
40 20
20 10
0 0
Time (MInutes)
200 178.4
150
100 83
50 31.1 31.5
8 8.5 0 00 00
0
Idling andBreakdown Set-up and Yield lossReduced speedDefects in
minor stoppage (failure loss) adjustment process
After reducing stoppage losses
Before reducing stoppage losses
6 Conclusions and recommendations for future ring cops. By applying Kaizen, the OEE of the ring frame
research section increased from 75.09 to 86.02%. The study can
further be extended in the following direction to shed more
Continuous improvement is essential for sustaining and light on TPM from the viewpoint of the textile and clothing
gaining a competitive advantage for manufacturing industries. industry:
As the textile spinning plant is a continuous processing unit,
the OEE depends on process stability as well as equipment • Section-wise Kaizen extension: We only focused on the
performance. The objective of this study was to examine the ring frame section of the spinning factory. Kaizen could
OEE of the ring frame section by identifying the related also be implemented in the winding, speed frame, draw
losses. Kaizen, one of the pillars of TPM, was applied to frame, and carding section to improve the OEE of these
improve the OEE of the ring frame. The six major sections.
stoppage losses identified in the manufacturing plant are • Possible implementation of rest of the TPM pillars:
breakdown or equipment failure, setup and adjustment, idling Apart from implementing Kaizen, other TPM pillars
and minor stoppage, reduced speed, de- fects in the process, such as autonomous maintenance [12]; planned
and reduced yield. The study revealed that Kaizen improved maintenance [46]; and safety, health, and environment
the productivity and enhanced the quality of [22] could be implemented in the factory in question.
1000
500
0
806.62
613.63