STS-41D National Space Transportation Systems Program Mission Report
Twelfth Space Shuttle flight and first flight of the OV-I03 vehicle, Discovery. This report summarizes the major activities and accomplishments of the mission. It also summarizes the significant problems that occurred during the launch scrub and launch abort. Four of the problems are of concern to The STS 41-G mission, and these are discussed in the latter portion of the report.
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STS-41D National Space Transportation Systems Program Mission Report
Twelfth Space Shuttle flight and first flight of the OV-I03 vehicle, Discovery. This report summarizes the major activities and accomplishments of the mission. It also summarizes the significant problems that occurred during the launch scrub and launch abort. Four of the problems are of concern to The STS 41-G mission, and these are discussed in the latter portion of the report.
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STS 41-D
National Space
Transportation Systems
Program Mission Report
September 1984
National Aeronautics and
Space Administration
Lyndon B. Johnson Space Center
Houston, Texas
JSC-20086TABLE OF CONTENTS
Title Page
INTRODUCTION AND MISSION OBJECTIVES
‘HISSION SUMMARY... ss
NT ee
‘SOLTD ROCKET BOOSTER . .
EXTERNAL TANK ss ee
SPACE SHUTTLE MAIN’ ENGINE
MAIN PROPULSION SYSTEM
ORBITER. we ee ee
CRT-2 Went Blank’ 1.)
7 laste Water Nozzle iced
en Tek ee cee ete ee
FUSE CEITT Pertorinnce Monitor indicator Faited
ficroswitch Anomalies see see ee ee eet
‘Vehicle Pulled to Right After Nose Gear Touchdown
Mt
SYNCOM SATELLITE, ve se ee eee eee ‘
TELSTAR 3-C SATELLITE Se ee 5
SOLAR ARRAY EXPERIMENT oes ee :
CONTINUOUS FLOW ELECTROPHORESIS SySTEM L211 t s
TMAX 7OMM CAMERA we oe ee ee 5
RADIATION MONITORING EQUIPMENT 2 ee ee 2
CLOUD PHOTOGRAPHY... ee ee ee eee 5
STUDENT EXPERIMENT oe vee eee eee aeINTRODUCTION AND MISSION OBJECTIVES
The STS 41-D National Space Transportation Systems Program Mission Report contains a
summary of the major activities and accomplishments of the twelfth Space Shuttle
flight and the first flight of the OV-103 vehicle, Discovery. This report also sun-
marizes the significant problems that occurred during the STS 41-0 launch scrub and
Jaunch abort, as well as the mission. The problem tracking list is presented to pro-
vide a compléte list of all Orbiter problems that occurred. Four of the problems are
of concern to the STS 41-G mission, and these are discussed in the latter portion of
‘the report.
The primary objectives of the STS 41-D mission were the deployment of the SYNCOM-IV,
Telstar 3-C, and SbS-D satellites; operation of the OAST-1 (Office of Aeronautics and
Space Technology-1) payload; and accomplishment of the functions of the Radiation
Monitoring Equipment (RME), the Continuous Flow Electrophoresis System (CFES III),
and the IMAX Camera, The Sequence of events for this mission are shown in table 1.
The problem tracking lists for the MSFC (Marshall Space Flight Center) elements and
the Orbiter are shown in tables II and II1, respectively, at the end of the report.
MISSION SUMMARY
The STS 41-D mission, the first for the OV-103 vehicle, Discovery, was scheduled for
Vaunch on June 25, 1984, and June 26, 1984, and August 29, 1984. ‘The attempted
launch on June 25, 1984, was scrubbed because GPC-5 (general purpose computer-5) ,
which contained the backup flight system software, exhibited two memory parity errors
at T-32 minutes, At T-20 minutes, the launch was scrubbed because the problem, which
was subsequently diagnosed as contamination of an integrated circuit, could not be
Corrected without hardware removal and replacement.
The launch was rescheduled for June 26, 1984, and all aspects of the countdown were
nominal until T-4 seconds when irregular operation of the main fuel valve on SSME~3
(Space Shuttle main engine 3) resulted in an engine shutdown (abort) condition, The
NSFC report entitled, STS 41-0 (14) Launch Attempt Report, dated July 3, 1984, con-
Banca eae rat ied STSCHsSTOG aT ERE Taunchcabores Asa result cf the aborts. the
decision was made to roll the vehicle back to the VAB (Vertical Assenbly Building)
and remanifest the mission, conbining the payloads from STS 41-F with STS 41-D, A
few launch date of August 29, 1984, was established. However, the launch was delayed
for 24 hours because of a timing problem between the flight software and the MEC
(master events controller). Tests showed that under certain worst case timing con~
ditions, the MEC would not process certain critical events conmands and, as a result,
could prevent separation of the SRB's and ET as well as other vital operations. A
Software patch was developed, tested, and incorporated in the vehicle computer soft-
ware to work around the timing problém, and allow the launch to proceed on August 30,
1984,
The final countdown again proceeded very smoothly for the planned Taunch at 8:36
a.me.d.t. However, the launch was delayed 6 minutes and 50 seconds at 1-9 minutes
because of a problem with the ground launch sequencer and two private aircraft that
were flying in the restricted area for launch operations. Lift-off occurred at
243:12:41:50 G.m,t. from Launch Complex 398 at KSC (Kennedy Space Center) on
August. 30, 1984, and the mission was successfully concluded with @ landing at Edwards
AFB (Air Force dase), at 249:13:37:54 G.m.t. on Septenber 5, 1984,The crew for this flight was Henry W. Hartsfield, Jr., Commander; Michael L. Coats,
Cdr, U.S. Navy, Pilots Dr. Steven A, Hawley, Richard M. Mullane, Lt. Col. USAF,
and’Or, dudith’A, Resnik, Mission Specialists; and Charles D. Walker, Payload
Specialist.
The ascent phase was normal in all respects. The SRB (solid rocket booster) head
pressures and burn rates were normal with SRB separation occurring within 0.14 second
of the predicted. Main propulsion system and engine performance were as predicted
with all thrust values indicating repeatable performance. MECO (main engine cut off)
occurred 0.3 second earlier than predicted, The orbital parameters at MECO were as
predicted. The OMS (orbital manuevering system) burns, -1 and -2, placed the vehicle
ina near circular orbit at 160 nautical miles.
The first day of STS 41-0 mission was very successful. The deploynent of the SBS
satellite was completed very smoothly and the 87-second firing of the PAM (payload
assist module) motor was completed satisfactorily. The failures that occurred the
first day were minor and had no impact on the flight. The most significant failures
were that CRT(cathode ray tube)-2 went blank and the fuel cell 1 CPM (cell perform-
ance monitor) ceased operating, The IFM (inflight maintenance) procedure for
placing CRT-8 in the CRT-2 position was performed on the fourth day. As a result of
the fuel cell 1 performance monitor failure, main bus A and 8 were tied together
during on-orbit operations so that fuel celi 1 and 2 performance could be compared.
The second day of the STS 41-0 mission was satisfactory with no new Orbiter anomalies
defined during the period, Payload deployment activities were nominal. The SYNCOM
satellite was successfully deployed using a technique referred to as a "frisbee
deploy". Also, SYNCOM was the first satellite specifically designed to fly on Space
Shuttle. All planned testing for the second day was satisfactorily completed.
The third day of the STS 41-D mission proceeded very smoothly with no new Orbiter
anomalies or problems defined during this period, All Orbiter subsystens continued
to operate satisfactorily. Deployment of the third satellite, Telstar, as well as
its perigee burn, were completed very satisfactorily. Postflight reports of the
three deployed satellites indicate all three are on station in the desired
geosynchronous orbit. The OAST/Solar Array Experiment operations were successful
with the array deployed to 70 percent for dynamic tests.
The fourth day of the STS 41-D was completed successfully. AI] planned payload
activities were accomplished and danping tests of the 100-percent deployed solar
array produced better than predicted results, thus allowing shopping list items to
be accomplished in addition to the planned items.
As_a result of the data review of the supply water dup at approximately 68 hours
MET (mission elapsed time), it was determined that fce had formed around the supply
dump nozzle. There also were indications that ice had formed around the waste water
dump nozzle, but it was believed that the ice did not remain. The RMS (remote mani-
pulator system) was deployed and the RMS TV showed a large column of ice over the
Supply nozzle. A waste dump was attempted with TV coverage; ice buildup was observed
and the waste dump was terminated,The Fifth day of the STS 41-0 mission was completed with all Orbiter subsystens and
experiment systems operating satisfactorily, but a major concern existed over the ice
formation on the supply and waste dunp nozztes. A TV scan showed that the amount of
ice was considerably less than the amount observed about 24 hours earlier. Primary
RCS (reaction control system) firings were performed in an unsuccessful attenpt to
dislodge the ice. The cabin was depressurized to 10.2 psia to provide for a poten-
tial contingency EVA (extravehicular activity) in the event the RMS operation was
unsuccessful in removing the ice. Subsequently, early on the sixth day, the RMS was
used to renove the ice from the supply dump nozzle, but the ice still remained on the
waste dump nozzle. The cabin was repressurized to’ 14.7 psia. A subsequent TV survey
of the dup nozzles after extended sun exposure and repeated nozzle heater cycles
showed that the remaining ice was essentially gone.
Al] planned OAST-1 activities were completed and the solar array was retracted and,
locked down. The crew completed the flight control system checkout using APU-2
(auxiliary power unit) satisfactorily. Final activities with the CFES (continuous
flow electrophoresis system) were ended just prior to the final sleep period with
85 percent of the samples processed.
The crew was awakened early on entry day because of an oxygen leak (about 30
pound/hour) in the environmental control and life support system. The crew performed
the necessary malfunction procedures and were able to isolate the leak and stop the
Flow of oxygen to that point. This leak did not impact the entry day activities, but
did cause the loss of redundancy in that system.
The crew completed all activities required for entry and performed the deorbit
maneuver at 249:12:36:20.2 G.m.t. The entry was normal and all PTI (programmed test
input) maneuvers were performed. After completing the HAC (heading alignment circle)
turn angle of 251 degrees, the Orbiter was guided to a landing at Edwards AFB.
Rollout required approximately 10,270 feet. An inspection after landing revealed the
right main gear strut had lost its pressure, a condition that caused the Orbiter to
pull to the right after nose gear touchdown. The STS 41-D mission was successfully
concluded at 249:13:38:54 G.m.t., when the Orbiter came to a stop on lakebed runway
EDWI7L. All 15 of the planned detailed test objectives had been successfully
accomplished,TABLE I, - STS 41-D SEQUENCE OF EVENTS
Event
Retual tine, Gombe
APU activation (1)
Q)
(3)
SRB HPU Activation command LH-A2
MPS start command sequence (engine 3)
‘SRB ignition command from GPC (lift-off)
MPS throttle down to 84-percent thrust (engine 3)
MPS throttle down to 65-percent thrust (engine 3)
Maximum dynamic pressure
MPS throttle up to 104-percent thrust (engine 3)
SRB separation command
WPS throttle down for 3g acceleration (engine 3)
Main engine cut off (MECO)
External tank separation
OMS-1 ignition
OMS-1 cutoff
APU deact fvation (1)
(2)
(3)
OMS-2 ignition
OMS-2 cutoff
SBS-D deploy
OMS-3 ignition
OMS-3 cutort
SYNCOM IV deploy
OMS-4 ignition
OMS-4 cutoff
TELSTAR 3-C deploy
ONS-5 ignition
OMS-5 cutoff
OMS-6 ignition
OMS-6 cutoff
OPS-8 (flight control system) checkout APU 2 activation
APU 2 deactivation
APU 3 activation
Deorbit maneuver ignition
Deorbit maneuver cutoff
APU 1 activation
APU 2 activation
Entry interface (400,000 ft)
End blackout
Terminal Area Energy Management: (TAEM)
Main landing gear contact (LH)
Nose landing gear contact
Wheels stop
APU deactivation completeVEHICLE ASSESSMENT
SOLID ROCKET BOOSTER
AN] Solid Rocket Booster (SRB) systems performed as expected. The SRB prelaunch
countdown Was nominal with no problems noted. Performance of both SRN's was near
predicted values and well within the allowed envelopes. Head pressures and pro-
pellant burn rates were as predicted. Thrust imbalance was within specification
throughout SRB operation. Preliminary indications are that the SRB's separated
approximately 0.14-second earlier than predicted.
The SRB recovery system operated nominally, with both SRB's reported to be floating
in the normal manner approximately 2.4 miles apart. Reports from the recovery ships
indicated that all main parachutes deployed. Both’ frustums were recovered, and also
all parachutes were recovered and had only minimal damage.
EXTERNAL TANK
ANI External Tank (ET) systems performed as expected. No TPS (thermal protection
system) anomalies were observed. Normal icing was reported in the waived areas, and
no acreage ice was reported. The only problem reported was the continued failure of
the two nose cone tenperature sensors that had failed on the earlier launch attenpts.
This problem had no effect on ET performance. All ul lage pressure transducers were
in the normal operating band throughout prepressurization and the flight. After
separation, the tumble was noted on tracking radars, and the impact was within the
planned footprint.
SPACE SHUTTLE MAIN ENGINE
AL] SSHE (Space Shuttle Main Engine) parameters appeared nominal during the prelaunch
countdown and compared well with prelaunch parameters that were observed during the
previous STS 41-D launch abort on June 26, 1984,
AN] valves functioned satisfactorily, meeting the newly adopted Launch Commit
Criteria (LCC). Performance at start, mainstage, shutdown and propel lant dump was
Satisfactory. The initial thrust buildup of main engine 3, although within specifi-
cation, was Slower than desired, HPFTP (high pressure fuel turbopump) and HPOTP
(high pressure oxidizer turbopump) temperatures appeared to be very close to predic-
tions. There were no anomalies identified.
MAIN PROPULSION SYSTEM
Overall performance of the MPS (Main Propulsion System) was excellent, both during
relaunch operations and the abort. LO2 and LH2 loading was accomplished as planned
with no stop flows or reverts. Propellent loads were near the predicted values.
There were no hazardous gas leaks of any significance.
The engine start buiTdups and transitions to mainstage were within specifications.
Engine operation and performance during mainstage appeared satisfactory. During
steady state performance, ET/088 pressures and temperatures and ORB/SSME pressures
and ratio and thrust values Tron the flight indicate repeatable engine performance.
Power level throttling operation appeared normal. Engine shutdown was satisfactory.
MECO occurred approximately 0.3 second earlier than predicted.ORBITER
CRT-2 Went Blank
At approximately 243:16:24 G.m.t, the crew reported that CRT-2 went blank, The OU
(display unit) and DEU (display electronics unit) BITE flags were on, and the DU
filament current error, DU power supply error, and DU deflection error BITE bits
were set. No current spikes at the time of the failure are discernible within the
granularity of the data,
Engineering analysis almost conclusively indicated that the failure was in the DU,
and that there was no mechanism by which a bad DEU could harm a replacement DU. An
inflight maintenance procedure, which required about 1 hour 15 minutes, was performed
to replace DU-2 with DU-4, The new DU operated normally.
Suppy/Waste Mater Nozzle Iced
During the third supply water dump, which included 8 percent from tank 8 and 20 per-
cent from tank A, the supply water nozzle temperature decreased from 20U° F to 38° F,
recovered to 80°'F, then peaked to 100° F and returned again to 80° F over a
19-minute period. "Nozzle temperatures that drop below 50° F are indicative of ice
format ion, Use of the RMS CCTV (closed circuit television) verified that ice had
formed around the supply water dump nozzle. The ice formation was approximately
12 ing in diameter and tapered to @ point about 27 in. in Tength from the side of the
vehicie.
Due to the ice formation, al] subsequent supply water dumps were deleted from the STS
41-D mission timeline and the flash evaporator system was used to manage that water.
A waste water dump was required and attemped on flight day 4 during live RMS CCTV
coverage. The waste water dump was discontinued after expelling about 5 - 7 percent
because of rapid ice buildup on the waste water nozzle. During the renainder of the
mission, the crew used available bags for urine collection, Adequate waste water
tank capacity existed for condensate collection.
A procedure was developed and successfully implemented to remove the ice from the
supply water nozzle using the RMS to impact and dislodge the ice formation. Due to
‘the proximity of the waste water nozzle to the wing, the waste water ice removal with
the RMS was not attempted. Positioning the vehicle for side sun and repeated heater
cycling resulted in the waste water ice being almost completely removed by flight day
i
The formation of ice during the third supply water dump resulted from ice particles
being trapped by the AFRSI/nozzle configuration and a large system pressure drop
which caused the water dump spray pattern to widen and come in contact with the ice
particles. Ice growth eminated from the ice particles back to the supply water
nozzle completely covering the nozzle,
Oxygen Leak
A cryogenic oxygen leak occurred downstream of the ECS (environmental control system)
supply isolation valve 2 on flight day 6. The Teak was about 30 pound/hour in excess
of the normal usage. The leak was isolated and stopped by closing ECS supply isola~
tion valve 2.Fuel Cell_1 Performance Monitor Indicator Failed
At approximately 243:18:35 Gm.t., the three cell-l-substack differential voltage
measurements from the performance monitor read zero. There was no indication of
power problems on any other equipment at that time indicating that the failure was
in the monitor and not the fuel cell, Buses A and B were tied together to permit
monitoring of fuel cell 1 performance by comparison of its load sharing with fuel
cell 2, The buses were untied prior to entry.
Microswitch Anomalies
Five anomalies occurred on STS 41-D in which the electrical circuits contained
microswitches of the same part number, These switch components are of the type
that had previously experienced failures because of contamination, Conductive
and non-conductive particles that are internal to the switches have caused both
false "open" and false “closed” indications.
The five circuits that were involved include:
a. The forward RCS (reaction control systen) manifold 2 fuel isolation valve
closed indication,
b. The aft right RCS’ fuel 3/4/5 crossfeed valve open indication.
c. The aft starboard payload bay door open indication.
4. The right OMS (orbital maneuvering system) crossfeed 8 fuel and oxidizer
valves open and closed indications,
fe. The right OMS fuel tank fsolation valve open indication,
These problems had no impact on mission operations.
Vehicle Pulled To Right After Nose Gear Touchdown
The STS 41-0 Commander reported during techincal debriefings that the vehicle
pulled to the right after nose gear touchdown. The Commander was able to control
the vehicle satisfactorily by applying as mich as 25 degrees of rudder. After the
vehicle reached about 120 knots, the Commander began differential braking, A
postflight inspection showed the right main gear shock strut was compressed to
within 0.5 in, of the fully compressed condition; whereas, the left main gear was
compressed to 2 nominal 3,5 in, The Schrader valve was found leaking gaseous
nitrogen, which in turn decreased the pneumatic pressure and caused the excessively
compressed strut. This low strut was responsible for the pulling-to-the-right
condition noted during rollout.
PAYLOADS AND EXPERIMENTS
SBS-D SATELLITE
The SBS-D satellite was deployed at 243:20:40:18 G.mst., within 1 second of the
Planned tine, The deployment was nominal in all respects and the closed-circuit
TV was used to monitor the deployment activities. The RMS television wrist camera
was used to document the perigee kick motor firing. The S8S-0 satellite has
Completed all major maneuvers and is now in geosynchronous orbit. The antennas and
solar panels are deployed and the checkout has been initiated. All aspects of the
Orbiter operation for this deployment were normal,