Power Plant Thermography - Part II: Mike Ralph Exelon Nuclear
Power Plant Thermography - Part II: Mike Ralph Exelon Nuclear
Mike Ralph
Exelon Nuclear
ABSTRACT
The infrared camera is a frequently used weapon in the integrated arsenal of Predictive Maintenance
technology. One of these cameras coupled with strong vibration and lubrication programs can help resolve
most equipment problems. Throw in some ultrasonic detection and a good process computer, and today's
PdM specialist is nearly invincible. This paper demonstrates some of the more interesting problems, and the
tools used to identify them and bring them to closure. Faults include a hot spot in a cable connection for a
large chiller, a hot bus bar connection in a critical panel, a complicated compressor issue, and a relatively
small hot spot on a terminal board that could have had severe consequences. Finding these issues early and
scheduling the repairs resulted in significant cost savings and prevented something else that executives and
investors both abhor surprise!
INTRODUCTION
Thermography is one of the mainstays of a strong PdM program. Not only is our program integrated with
other predictive technologies such as vibration and lubrication analysis, it is included in a total effort to
promote maintenance optimization. Once a problem is detected and diagnosed, often using multiple
technologies, a comprehensive approach eliminates the possibility of recurrence and improves the efficiency
of maintenance performed in the future. Our goal is not only to prevent failure, but also to exploit
opportunities for improved cost effectiveness. Achieving this goal requires intense record retention in the
form of case histories. Here are some examples from the component health database.
THERMOGRAPHIC OBSERVATION
Figure 1 includes the IR images of the B-phase main power supply connections on the D Turbine Building
Chiller. Delta-T between phases trended up to 57 F. This made it yellow or alert range in the component
health-tracking program. We assumed that the temperature was higher given the insulating wrap installed on
the connection.
154.3F 98.3F
95
140
90
120 85
80
100
75
86.2F 72.5F
106.9F 252.1F
250
100
200
90
150
80
100
74.3F 75.1F
SUMMARY
This connection would not fail at or below measured temperatures of 600F, which helped to establish an
absolute upper limit for monitoring the connection until the outage began. Thermal testing increased in
frequency, and occurred daily until repairs could be performed. Fortunately, the temperature remained stable
until repairs were completed. Electrical maintenance technicians removed the degraded hardware, cleaned
the connection and installed a new bolt on the lug assembly. Our typical scheduling period for predictive
issues requiring repair during a refuel outage is greater than one year. Unfortunately, we did not meet that
goal in this instance. However, we did identify a potentially serious problem that would likely have resulted in
lost production.
Between February 17, 2005 and March 14th, 2005 seal air pressure as indicated by local gauge and trended
with vibration had increased to 32 psig, which is above the vendor recommended specification for continued
operation. Vibration analysis indicated that all stages were operating acceptably. However, the vibration
level on the fourth stage (49,000 rpm) had trended down to about 50% of the amplitude seen one year earlier,
and the analyst had questioned whether the proximity probe was functioning correctly. The frequency
response and gap voltage were normal. This would become a key observation as the investigation continued.
Thermography indicated normal conditions comparable to the other compressors as indicated in Figure 2,
Stage #2
200 200
150 150
Stage #4
Stage #3
100 100
86.0F 86.0F
Figure 2. Thermogram Stage 2 & 3 on the left and Stages 3 & 4 on the right. Stage #4 measured 228F
Figure 3 below demonstrates the downward trend observed prior to the increase in seal air noted in March of
2005. Vibration levels remained normal on three of the four stages, with the only abnormality being the
downward trend on Stage #4. A contingency work order had been prepared earlier based on concern for the
downward vibration trend and some previous observations on another compressor train.
.12 Mils
Date: 15-Mar-05
0 100 200 300 400 500 600 700 800 Time: 12:59:02
Days: 03-Mar-03 To 11-Apr-05 Amp4: .138
Figure 3. Vibration level on stage four, the highest rpm stage trended downward 50% over one year. Note that
after the compressor rebuild, all values changed establishing a new baseline.
During disassembly and inspection, we noted that the journals of the rotors, especially on Stage #4 and to a
lesser degree on Stage #3, were discolored. A brown material had built up on the rotor and was assumed
that it was oil residue. Laboratory analysis of the material indicated it was composed primarily of
phosphorous and zinc. This machine has a central lubrication system utilizing synthetic oil. This same type
of oil had been used in the machine for over 15 years with no previous adverse effect, but phosphorous and
zinc were a prevalent part of the additive package for this type of oil.
SUMMARY
When all of the facts were gathered, we determined that a change in the additive package for the oil was the
root cause of the degradation experienced on this compressor. The change in the formulation had occurred
many years earlier and had been properly communicated by the vendor, but we did not recognize that it
would be detrimental to this type of machine. The amount of phosphorous additive was doubled during the
formulation change. Since oil at our station is changed out based on analysis, the effects of the formulation
change were not felt until an oil change out occurred late in 2003.
While the viscosity of synthetic lubricants will remain stable in a high temperature environment, sustained high
temperature can cause additives to plate out on hot surfaces, causing varnish. The vast majority of rotating
equipment would not experience a problem, but centrifugal air compressor rotors operate at extreme speeds
and the bearing clearances are tight at ~0.003 diametric. The layer of varnish actually displaced the limited
bearing clearance that was available, causing the vibration amplitude to trend down over time. When the
clearances became too tight, the bearing wiped and damaged the air seal causing air seal pressure to
increase above the limit.
This was a good example of using all the PdM tools available, including work history, to diagnose a problem
and provide a permanent solution. The oil was changed to a mineral based type of the same viscosity with
little or no additives. The frequency of oil changes may increase, but reliability of the compressors has
improved.
84
82
80
78.9F
SUMMARY
During inspection electricians found the terminal screw loose approximately one-quarter turn. Temperature
on the connection returned to normal after corrective maintenance was completed.